HL incident on 2018-11-21 — TX

Operator
Sunoco Partners Marketing & Terminals Lp
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2018-11-21 15:57
Report number
Location
TX
Narrative
At approximately 11:30 on 11/21/2018, a release of approximately 3 bbl. Of crude oil was discovered from the texoma manifold #2 suction barrel. Operations stopped pumping and isolated the suction barrel. The immediate leak was located and contained and a vacuum truck and osro were called in to remove the oil and water from the texoma manifold area. Previously installed repair clamp on the suction line was found to be loose. Root cause was determined to be thermal stress on this above ground section of pipe due to recent inclement cold weather which caused contraction of pipe and affected torque of repair clamp bolts. Mechanics were able to retighten bolts and stop release. Working with scheduling for downtime to make permanent repairs. No environmental implications. There was water in the basin of the manifold area as a result of recent rain. The crude remained suspended from the ground via the water and there was no soil impacted.
Detailed record list
Report Received Date
2018-12-20 00:00:00
Iyear
2018
Report Number
20180399
Supplemental Number
31369
Report Type
Original Final
Operator Id
Name
Sunoco Partners Marketing & Terminals Lp
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-11-21 15:57:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-11-21 15:57:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Area Was Bypassed And Locked Out While Repairs Were Made
On Site Datetime
2018-11-21 15:57:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Nederland Terminal
Segment Name
Texoma Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Repair Sleeve Or Clamp
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
210
Est Cost Prop Damage
200
Est Cost Emergency
11840
Est Cost Environmental
2700
Est Cost Other
0
Prpty
14950
Accident Psig
25
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Temperature Subtype
Thermal Stress
Nf Extreme Weather Ind
No
Preparer Name
T*** N*******
Preparer Title
Sr. Manager - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2018-12-20 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Sr. Manager - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
At approximately 11:30 on 11/21/2018, a release of approximately 3 bbl. Of crude oil was discovered from the texoma manifold #2 suction barrel. Operations stopped pumping and isolated the suction barrel. The immediate leak was located and contained and a vacuum truck and osro were called in to remove the oil and water from the texoma manifold area. Previously installed repair clamp on the suction line was found to be loose. Root cause was determined to be thermal stress on this above ground section of pipe due to recent inclement cold weather which caused contraction of pipe and affected torque of repair clamp bolts. Mechanics were able to retighten bolts and stop release. Working with scheduling for downtime to make permanent repairs. No environmental implications. There was water in the basin of the manifold area as a result of recent rain. The crude remained suspended from the ground via the water and there was no soil impacted.
Report Received Date 2018-12-20 00:00:00
Iyear 2018
Report Number 20180399
Supplemental Number 31369
Report Type Original Final
Operator Id 39706 PHMSA Enforcement
Name Sunoco Partners Marketing & Terminals Lp
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-11-21 15:57:00
Location Latitude 29.991667 Google Maps OpenStreetMap
Location Longitude -93.991388 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-11-21 15:57:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Area Was Bypassed And Locked Out While Repairs Were Made
On Site Datetime 2018-11-21 15:57:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Nederland Terminal
Segment Name Texoma Manifold
Onshore State Abbreviation Tx
Onshore Postal Code 77627
Onshore City Name Nederland
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Repair Sleeve Or Clamp
Installation Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 210
Est Cost Prop Damage 200
Est Cost Emergency 11840
Est Cost Environmental 2700
Est Cost Other 0
Prpty 14950
Accident Psig 25
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Temperature Subtype Thermal Stress
Nf Extreme Weather Ind No
Preparer Name T*** N*******
Preparer Title Sr. Manager - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2018-12-20 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Sr. Manager - Dot Compliance
Authorizer Email T************@e*************.com
Narrative At approximately 11:30 on 11/21/2018, a release of approximately 3 bbl. Of crude oil was discovered from the texoma manifold #2 suction barrel. Operations stopped pumping and isolated the suction barrel. The immediate leak was located and contained and a vacuum truck and osro were called in to remove the oil and water from the texoma manifold area. Previously installed repair clamp on the suction line was found to be loose. Root cause was determined to be thermal stress on this above ground section of pipe due to recent inclement cold weather which caused contraction of pipe and affected torque of repair clamp bolts. Mechanics were able to retighten bolts and stop release. Working with scheduling for downtime to make permanent repairs. No environmental implications. There was water in the basin of the manifold area as a result of recent rain. The crude remained suspended from the ground via the water and there was no soil impacted.

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