HL incident on 2018-11-29 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$20,000
Incident datetime
2018-11-29 18:53
Report number
Location
TX
Narrative
On 11/29/2018 at 18:53 while lo01 was running in steady state elk city unit 2 shut down on suction pressure low low. The line was immediately shutdown and blocked in. The field, lead and supervisor were notified. Field dispatched to investigate. Release was confirmed by field personnel at app. 10:15. Notifications were made and emergency response activities initiated. Release was due to failure of the long seam. Pipe segment was cut out and replaced on 12-1-2018. Line was recommissioned and returned to service on 12-2-2018. Removed section of piping was sent to lab for metallurgical analysis. G5, item #4 "additional factors" is undetermined for now until the metallurgical analysis is complete. The report will be supplemented upon establishment of failure mode. 2019-02-04 - updated part g, section 5, questions 1, 2, 4 and 5a bases on receipt of draft metallurgical analysis results on 1-25-2019. Updated part e, question 9. Preliminary metallurgical analysis indicates the failure was due to operational pressure cycle fatigue growth that originated from an internal hook crack manufacturing defect. 2019-4-1 - updated part e, items 1 and 2 with more accurate pressure at the point and time of failure and mop at the point and time of failure, per PHMSA request.
Detailed record list
Report Received Date
2018-12-20 00:00:00
Iyear
2018
Report Number
20180396
Supplemental Number
31881
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2018-11-29 18:53:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
672
Recovered Bbls
672
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2018-11-29 18:53:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-11-29 18:56:00
Restart Datetime
2018-12-02 17:45:00
On Site Datetime
2018-11-29 22:15:00
Nrc Rpt Datetime
2018-11-29 20:11:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Lo-01, Line O
Segment Name
Elk City To State Line
Onshore State Abbreviation
Ok
Onshore Postal Code
73644
Onshore City Name
Elk City
Onshore County Name
Beckham
Designated Location
Milepost/valve Station
Designated Name
Mp 116
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
28
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
10
Pipe Wall Thickness
0.203
Pipe Smys
42000
Pipe Specification
Api5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic
Pipe Coating Type
Coal Tar
Installation Year
1951
Manufactured Year
1951
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
1.5
Rupture Length
27.5
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
10000
Est Cost Gas Released
25000
Est Cost Prop Damage
20000
Est Cost Emergency
400000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
460000
Accident Psig
1106.7
Mop Psig
1117
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
187500
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Fatigue Vibr Related
Yes
Failure Subtype
Pressure-Related
Additional Crack Ind
Yes
Collected Data Ind
Yes
Emat Ind
Yes
Emat Recent Year
2014
Other Recent Year
2016
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2006
Hydrtst Most Rcnt Pressure
1500
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J*** B*********
Preparer Title
Dot Coordinator
Preparer Email
J**************@p**.com
Preparer Telephone
580-767-4206
Prepared Date
2019-04-01 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Dot Director
Authorizer Email
T***********@p**.com
Narrative
On 11/29/2018 at 18:53 while lo01 was running in steady state elk city unit 2 shut down on suction pressure low low. The line was immediately shutdown and blocked in. The field, lead and supervisor were notified. Field dispatched to investigate. Release was confirmed by field personnel at app. 10:15. Notifications were made and emergency response activities initiated. Release was due to failure of the long seam. Pipe segment was cut out and replaced on 12-1-2018. Line was recommissioned and returned to service on 12-2-2018. Removed section of piping was sent to lab for metallurgical analysis. G5, item #4 "additional factors" is undetermined for now until the metallurgical analysis is complete. The report will be supplemented upon establishment of failure mode. 2019-02-04 - updated part g, section 5, questions 1, 2, 4 and 5a bases on receipt of draft metallurgical analysis results on 1-25-2019. Updated part e, question 9. Preliminary metallurgical analysis indicates the failure was due to operational pressure cycle fatigue growth that originated from an internal hook crack manufacturing defect. 2019-4-1 - updated part e, items 1 and 2 with more accurate pressure at the point and time of failure and mop at the point and time of failure, per PHMSA request.
Report Received Date 2018-12-20 00:00:00
Iyear 2018
Report Number 20180396
Supplemental Number 31881
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2018-11-29 18:53:00
Location Latitude 35.443915 Google Maps OpenStreetMap
Location Longitude -99.387162 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 672
Recovered Bbls 672
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2018-11-29 18:53:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-11-29 18:56:00
Restart Datetime 2018-12-02 17:45:00
On Site Datetime 2018-11-29 22:15:00
Nrc Rpt Datetime 2018-11-29 20:11:00
Nrc Rpt Num 1231662 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Lo-01, Line O
Segment Name Elk City To State Line
Onshore State Abbreviation Ok
Onshore Postal Code 73644
Onshore City Name Elk City
Onshore County Name Beckham
Designated Location Milepost/valve Station
Designated Name Mp 116
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 28
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 10
Pipe Wall Thickness 0.203
Pipe Smys 42000
Pipe Specification Api5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Republic
Pipe Coating Type Coal Tar
Installation Year 1951
Manufactured Year 1951
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 1.5
Rupture Length 27.5
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 10000
Est Cost Gas Released 25000
Est Cost Prop Damage 20000
Est Cost Emergency 400000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 460000
Accident Psig 1106.7
Mop Psig 1117
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 187500
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Fatigue Vibr Related Yes
Failure Subtype Pressure-Related
Additional Crack Ind Yes
Collected Data Ind Yes
Emat Ind Yes
Emat Recent Year 2014
Other Recent Year 2016
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2006
Hydrtst Most Rcnt Pressure 1500
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J*** B*********
Preparer Title Dot Coordinator
Preparer Email J**************@p**.com
Preparer Telephone 580-767-4206
Prepared Date 2019-04-01 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Dot Director
Authorizer Email T***********@p**.com
Narrative On 11/29/2018 at 18:53 while lo01 was running in steady state elk city unit 2 shut down on suction pressure low low. The line was immediately shutdown and blocked in. The field, lead and supervisor were notified. Field dispatched to investigate. Release was confirmed by field personnel at app. 10:15. Notifications were made and emergency response activities initiated. Release was due to failure of the long seam. Pipe segment was cut out and replaced on 12-1-2018. Line was recommissioned and returned to service on 12-2-2018. Removed section of piping was sent to lab for metallurgical analysis. G5, item #4 "additional factors" is undetermined for now until the metallurgical analysis is complete. The report will be supplemented upon establishment of failure mode. 2019-02-04 - updated part g, section 5, questions 1, 2, 4 and 5a bases on receipt of draft metallurgical analysis results on 1-25-2019. Updated part e, question 9. Preliminary metallurgical analysis indicates the failure was due to operational pressure cycle fatigue growth that originated from an internal hook crack manufacturing defect. 2019-4-1 - updated part e, items 1 and 2 with more accurate pressure at the point and time of failure and mop at the point and time of failure, per PHMSA request.

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