HL incident on 2018-11-18 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,300
Incident datetime
2018-11-18 13:00
Report number
Location
TX
Narrative
During an operator round product was found outside of containment impacting the ground and retention pond with a diesel odor. The 13.88bbl release occurred over a 14.75 hr. Period. Investigation discovered an open integrity verification valve on a closed general twin seal valve. This allowed product to impact a sump cup that plugged and overflowed resulting in product impacting the ground and retention pond. The general twin seal was 1.5 turns from being 100% closed. At some point product began to pass through the valve seal, out the open integrity verification valve, through the open drain line and enter the sump. Historical sump activity indicates the drain line plugged and backed product through the open cup and onto the ground.
Detailed record list
Report Received Date
2018-12-20 00:00:00
Iyear
2018
Report Number
20180394
Supplemental Number
31592
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2018-11-18 13:00:00
Location Latitude
Location Longitude
-94.88635038
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
13.88
Recovered Bbls
13.88
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-11-18 13:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shutdown ~1hr After Discovery. Diesel Was Initially Reported Then Gasoline.
On Site Datetime
2018-11-18 13:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Gold Line
Segment Name
Gd02
Onshore State Abbreviation
Ks
Onshore Postal Code
66071
Onshore City Name
Not Within A Municipality
Onshore County Name
Miami
Designated Location
Milepost/valve Station
Designated Name
Paola Termina
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Opensump Drain Line Became Plugged
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Open Sump Drain Line Plugged And Overfilled Onto Ground.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1034
Est Cost Prop Damage
15300
Est Cost Emergency
23000
Est Cost Environmental
12000
Est Cost Other
0
Est Cost Other Details
All Other Cost Totals Are Not Currently Available.
Prpty
51334
Accident Psig
136
Mop Psig
1190
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The nature of the release could not have been discovered by control center personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Operator Closed The Valve But Failed To Seat The General Twin Seal Valve.
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
T** J****
Preparer Title
Dot Coordinator
Preparer Email
T**********@p**.com
Preparer Telephone
918-977-4358
Prepared Date
2019-02-01 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
8327651632
Authorizer Title
Director Dot Compliance
Authorizer Email
M***********@p**.com
Narrative
During an operator round product was found outside of containment impacting the ground and retention pond with a diesel odor. The 13.88bbl release occurred over a 14.75 hr. Period. Investigation discovered an open integrity verification valve on a closed general twin seal valve. This allowed product to impact a sump cup that plugged and overflowed resulting in product impacting the ground and retention pond. The general twin seal was 1.5 turns from being 100% closed. At some point product began to pass through the valve seal, out the open integrity verification valve, through the open drain line and enter the sump. Historical sump activity indicates the drain line plugged and backed product through the open cup and onto the ground.
Report Received Date 2018-12-20 00:00:00
Iyear 2018
Report Number 20180394
Supplemental Number 31592
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2018-11-18 13:00:00
Location Latitude 38.50710998 Google Maps OpenStreetMap
Location Longitude -94.88635038 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 13.88
Recovered Bbls 13.88
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-11-18 13:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shutdown ~1hr After Discovery. Diesel Was Initially Reported Then Gasoline.
On Site Datetime 2018-11-18 13:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Gold Line
Segment Name Gd02
Onshore State Abbreviation Ks
Onshore Postal Code 66071
Onshore City Name Not Within A Municipality
Onshore County Name Miami
Designated Location Milepost/valve Station
Designated Name Paola Termina
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Opensump Drain Line Became Plugged
Installation Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Open Sump Drain Line Plugged And Overfilled Onto Ground.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1034
Est Cost Prop Damage 15300
Est Cost Emergency 23000
Est Cost Environmental 12000
Est Cost Other 0
Est Cost Other Details All Other Cost Totals Are Not Currently Available.
Prpty 51334
Accident Psig 136
Mop Psig 1190
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The nature of the release could not have been discovered by control center personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Operator Closed The Valve But Failed To Seat The General Twin Seal Valve.
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name T** J****
Preparer Title Dot Coordinator
Preparer Email T**********@p**.com
Preparer Telephone 918-977-4358
Prepared Date 2019-02-01 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 8327651632
Authorizer Title Director Dot Compliance
Authorizer Email M***********@p**.com
Narrative During an operator round product was found outside of containment impacting the ground and retention pond with a diesel odor. The 13.88bbl release occurred over a 14.75 hr. Period. Investigation discovered an open integrity verification valve on a closed general twin seal valve. This allowed product to impact a sump cup that plugged and overflowed resulting in product impacting the ground and retention pond. The general twin seal was 1.5 turns from being 100% closed. At some point product began to pass through the valve seal, out the open integrity verification valve, through the open drain line and enter the sump. Historical sump activity indicates the drain line plugged and backed product through the open cup and onto the ground.

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