HL incident on 2018-12-06 — TX

Operator
Rose Rock Midstream L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2018-12-06 15:05
Report number
Location
TX
Narrative
On december 6th, 2018 at approximately 3:05 pm cst, oil that had leaked near and around tank 2535 was discovered. Upon further investigation the source of the crude oil leak was from the seal on the northwest mixer. The crude oil had accumulated primarily on the west side of tank 2535 and had migrated in low lying areas around the tank to the northeast and southwest. Approximately 28 barrels of crude oil was released, the volume of the release was determined by scada information and the amount of product recovered. Company personnel were able to stop the release by placing the mixer in a maintenance mode. Emergency response and clean up efforts were conducted by company personnel and contract personnel under the direction of the maintenance supervisor. Air monitoring was on site continuously throughout the clean up to ensure benzene levels were safe and all readings were less than the action level. The initial clean up was concluded at 10 pm cst on dec. 6th. Clean up efforts to restore the impacted area were completed by dec. 11th.
Detailed record list
Report Received Date
2018-12-14 00:00:00
Iyear
2018
Report Number
20180388
Supplemental Number
31328
Report Type
Original Final
Operator Id
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-12-06 15:05:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
28
Recovered Bbls
26
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-12-06 15:05:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Isolated To Breakout Tank Involved.
On Site Datetime
2018-12-06 15:05:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Terminal
Segment Name
Tank 2535
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Not Within A Municipality
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Breakout Tank
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Tank Type
Atmospheric
Item Involved Details
Mixer
Installation Year
2009
Material Involved
Material Other Than Carbon Steel
Material Details
Mixer Seal Surface
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
500
Est Cost Emergency
24915
Est Cost Environmental
5000
Est Cost Other
0
Prpty
30515
Accident Psig
15
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The accident was due to equipment failure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Seal Failure Due To Normal Wear And Tear.
Preparer Name
E*** N********
Preparer Title
District Manager
Preparer Email
E*********@s***********.com
Preparer Telephone
9183066016
Prepared Date
2018-12-14 00:00:00
Authorizer Name
L*** V******
Authorizer Telephone
9185248109
Authorizer Title
Dot Compliance Manager
Authorizer Email
L*******@s***********.com
Narrative
On december 6th, 2018 at approximately 3:05 pm cst, oil that had leaked near and around tank 2535 was discovered. Upon further investigation the source of the crude oil leak was from the seal on the northwest mixer. The crude oil had accumulated primarily on the west side of tank 2535 and had migrated in low lying areas around the tank to the northeast and southwest. Approximately 28 barrels of crude oil was released, the volume of the release was determined by scada information and the amount of product recovered. Company personnel were able to stop the release by placing the mixer in a maintenance mode. Emergency response and clean up efforts were conducted by company personnel and contract personnel under the direction of the maintenance supervisor. Air monitoring was on site continuously throughout the clean up to ensure benzene levels were safe and all readings were less than the action level. The initial clean up was concluded at 10 pm cst on dec. 6th. Clean up efforts to restore the impacted area were completed by dec. 11th.
Report Received Date 2018-12-14 00:00:00
Iyear 2018
Report Number 20180388
Supplemental Number 31328
Report Type Original Final
Operator Id 31476 PHMSA Enforcement
Name Rose Rock Midstream L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-12-06 15:05:00
Location Latitude 36.014722 Google Maps OpenStreetMap
Location Longitude -96.755556 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 28
Recovered Bbls 26
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-12-06 15:05:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Isolated To Breakout Tank Involved.
On Site Datetime 2018-12-06 15:05:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing Terminal
Segment Name Tank 2535
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Not Within A Municipality
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Breakout Tank
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Tank Type Atmospheric
Item Involved Details Mixer
Installation Year 2009
Material Involved Material Other Than Carbon Steel
Material Details Mixer Seal Surface
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 500
Est Cost Emergency 24915
Est Cost Environmental 5000
Est Cost Other 0
Prpty 30515
Accident Psig 15
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The accident was due to equipment failure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Seal Failure Due To Normal Wear And Tear.
Preparer Name E*** N********
Preparer Title District Manager
Preparer Email E*********@s***********.com
Preparer Telephone 9183066016
Prepared Date 2018-12-14 00:00:00
Authorizer Name L*** V******
Authorizer Telephone 9185248109
Authorizer Title Dot Compliance Manager
Authorizer Email L*******@s***********.com
Narrative On december 6th, 2018 at approximately 3:05 pm cst, oil that had leaked near and around tank 2535 was discovered. Upon further investigation the source of the crude oil leak was from the seal on the northwest mixer. The crude oil had accumulated primarily on the west side of tank 2535 and had migrated in low lying areas around the tank to the northeast and southwest. Approximately 28 barrels of crude oil was released, the volume of the release was determined by scada information and the amount of product recovered. Company personnel were able to stop the release by placing the mixer in a maintenance mode. Emergency response and clean up efforts were conducted by company personnel and contract personnel under the direction of the maintenance supervisor. Air monitoring was on site continuously throughout the clean up to ensure benzene levels were safe and all readings were less than the action level. The initial clean up was concluded at 10 pm cst on dec. 6th. Clean up efforts to restore the impacted area were completed by dec. 11th.

All rights reserved. Copyright © by ClearPHMSA