HL incident on 2018-11-06 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2018-11-06 18:40
Report number
Location
TX
Narrative
On 11/06/2018 at 18:40, baytown operations personnel noticed a small leak on sm102 pig trap closure mechanism inside the facility. Pipeline control was notified and closed a valve to isolate the pig trap. At 19:20, a pipeline technician depressurized the pig trap and inspected the closure mechanism to find the o-ring had failed. Visual examination of the o-ring indicates it broke where the ends of the o-ring was fused. To prevent recurrence, a td williams o-ring was installed on the td williams closure on 11/07/2018 on 11/06/2018 at 20:45, enterprise determined the release was a reportable accident based on the estimated volume release exceeding five (5) gallons. The trrc was called on 11/06/2018 at 21:10 hrs, incident #1876.
Detailed record list
Report Received Date
2018-12-03 00:00:00
Iyear
2018
Report Number
20180374
Supplemental Number
31853
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-11-06 18:40:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
1
Intentional Release Bbls
10
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-11-06 18:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Control Isolated Pig Trap
On Site Datetime
2018-11-06 18:40:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Shoup To Mont Belvieu
Segment Name
Sm102
Onshore State Abbreviation
Tx
Onshore Postal Code
77520
Onshore City Name
Baytown
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
10.33
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Viton O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1500
Accident Psig
1220
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
60
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pig trap closure mechanism is a manual operation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Failed Where The Ends Were Fused.
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
7133813536
Prepared Date
2019-03-27 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
7133812493
Authorizer Title
Compliance Manager
Authorizer Email
T*******@e****.com
Narrative
On 11/06/2018 at 18:40, baytown operations personnel noticed a small leak on sm102 pig trap closure mechanism inside the facility. Pipeline control was notified and closed a valve to isolate the pig trap. At 19:20, a pipeline technician depressurized the pig trap and inspected the closure mechanism to find the o-ring had failed. Visual examination of the o-ring indicates it broke where the ends of the o-ring was fused. To prevent recurrence, a td williams o-ring was installed on the td williams closure on 11/07/2018 on 11/06/2018 at 20:45, enterprise determined the release was a reportable accident based on the estimated volume release exceeding five (5) gallons. The trrc was called on 11/06/2018 at 21:10 hrs, incident #1876.
Report Received Date 2018-12-03 00:00:00
Iyear 2018
Report Number 20180374
Supplemental Number 31853
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-11-06 18:40:00
Location Latitude 29.76709 Google Maps OpenStreetMap
Location Longitude -95.01199 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 1
Intentional Release Bbls 10
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-11-06 18:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Control Isolated Pig Trap
On Site Datetime 2018-11-06 18:40:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Shoup To Mont Belvieu
Segment Name Sm102
Onshore State Abbreviation Tx
Onshore Postal Code 77520
Onshore City Name Baytown
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 10.33
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Scraper/pig Trap
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Viton O-Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1500
Accident Psig 1220
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 60
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pig trap closure mechanism is a manual operation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Failed Where The Ends Were Fused.
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 7133813536
Prepared Date 2019-03-27 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 7133812493
Authorizer Title Compliance Manager
Authorizer Email T*******@e****.com
Narrative On 11/06/2018 at 18:40, baytown operations personnel noticed a small leak on sm102 pig trap closure mechanism inside the facility. Pipeline control was notified and closed a valve to isolate the pig trap. At 19:20, a pipeline technician depressurized the pig trap and inspected the closure mechanism to find the o-ring had failed. Visual examination of the o-ring indicates it broke where the ends of the o-ring was fused. To prevent recurrence, a td williams o-ring was installed on the td williams closure on 11/07/2018 on 11/06/2018 at 20:45, enterprise determined the release was a reportable accident based on the estimated volume release exceeding five (5) gallons. The trrc was called on 11/06/2018 at 21:10 hrs, incident #1876.

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