HL incident on 2018-11-02 — TX

Operator
Sfpp, Lp
Cause
Locating Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50,000
Incident datetime
2018-11-02 11:20
Report number
Location
TX
Narrative
At 11:20 a.M. On 11/2/2018, a 3rd party contractor called the rocklin control room reporting they had just struck a pipeline with an auger while conducting geotechnical surveys along the railroad right of way. It was determined that ls-48 had been struck and diesel was released from the line as the static pressure in the line dropped from 70 psi to 0. The line was excavated, purged, and the damaged portion cut out and replaced with a new piece. After successful static and running tests, the line was returned to normal service and remediation activities continued for several weeks afterward until the majority of the contaminated soil had been removed to the extent practicable. An investigation into the accident revealed that ls-48 did not have proper markings at the time of the initial locate or at the time of the incident, however, the parallel sfpp ls-20 was properly marked. 1/30/2019 update- no edits or additions from original. Final supplemental submitted.
Detailed record list
Report Received Date
2018-11-30 00:00:00
Iyear
2018
Report Number
20180372
Supplemental Number
31579
Report Type
Supplemental Final
Operator Id
Name
Sfpp, Lp
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-11-02 11:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
77.49
Recovered Bbls
77.49
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2018-11-02 11:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Static At Time Of Incident And Not Scheduled To Deliver During Incident
On Site Datetime
2018-11-02 14:30:00
Nrc Rpt Datetime
2018-11-02 11:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Ls-48
Segment Name
Rocklin To Uprr
Onshore State Abbreviation
Ca
Onshore Postal Code
95678
Onshore City Name
Roseville
Onshore County Name
Placer
Designated Location
Milepost/valve Station
Designated Name
2.64
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Pipe Wall Thickness
0.188
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic
Pipe Coating Type
Extruded Polyehylene
Installation Year
1962
Manufactured Year
1962
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
4
Puncture Circum
3
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
941
Est Cost Prop Damage
50000
Est Cost Emergency
130000
Est Cost Environmental
223000
Est Cost Other
0
Prpty
403941
Accident Psig
70
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
19747
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was caused by 3rd party damage and controller's actions were eliminated as a cause or contributing factor
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Contractor Ind
Yes
Notify Cga Dirt
No
Railroad Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Engineering/surveying
One Call Notified Ind
Yes
One Call Ticket Num
829002051
Locator Type
Utility Owner
Visible Marks
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Marked Inaccurately Due To Locator Error
Preparer Name
W*** S******
Preparer Title
Pipeline Technical Specialist
Preparer Email
W***********@k***********.com
Preparer Telephone
661-304-6971
Prepared Date
2019-01-30 00:00:00
Authorizer Name
Q****** F******
Authorizer Telephone
770-751-4240
Authorizer Title
Director Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
At 11:20 a.M. On 11/2/2018, a 3rd party contractor called the rocklin control room reporting they had just struck a pipeline with an auger while conducting geotechnical surveys along the railroad right of way. It was determined that ls-48 had been struck and diesel was released from the line as the static pressure in the line dropped from 70 psi to 0. The line was excavated, purged, and the damaged portion cut out and replaced with a new piece. After successful static and running tests, the line was returned to normal service and remediation activities continued for several weeks afterward until the majority of the contaminated soil had been removed to the extent practicable. An investigation into the accident revealed that ls-48 did not have proper markings at the time of the initial locate or at the time of the incident, however, the parallel sfpp ls-20 was properly marked. 1/30/2019 update- no edits or additions from original. Final supplemental submitted.
Report Received Date 2018-11-30 00:00:00
Iyear 2018
Report Number 20180372
Supplemental Number 31579
Report Type Supplemental Final
Operator Id 18092 PHMSA Enforcement
Name Sfpp, Lp
Operator Street Address 1001 Louisiana St., Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-11-02 11:20:00
Location Latitude 38.7556 Google Maps OpenStreetMap
Location Longitude -121.27675 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 77.49
Recovered Bbls 77.49
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2018-11-02 11:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Static At Time Of Incident And Not Scheduled To Deliver During Incident
On Site Datetime 2018-11-02 14:30:00
Nrc Rpt Datetime 2018-11-02 11:59:00
Nrc Rpt Num 1229268 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Ls-48
Segment Name Rocklin To Uprr
Onshore State Abbreviation Ca
Onshore Postal Code 95678
Onshore City Name Roseville
Onshore County Name Placer
Designated Location Milepost/valve Station
Designated Name 2.64
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Pipe Wall Thickness 0.188
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Republic
Pipe Coating Type Extruded Polyehylene
Installation Year 1962
Manufactured Year 1962
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 4
Puncture Circum 3
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 941
Est Cost Prop Damage 50000
Est Cost Emergency 130000
Est Cost Environmental 223000
Est Cost Other 0
Prpty 403941
Accident Psig 70
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 19747
Internal Inspection Ind No
Tight Mitered Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was caused by 3rd party damage and controller's actions were eliminated as a cause or contributing factor
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Contractor Ind Yes
Notify Cga Dirt No
Railroad Row Ind Yes
Excavator Type Contractor
Excavator Equipment Auger
Work Performed Engineering/surveying
One Call Notified Ind Yes
One Call Ticket Num 829002051
Locator Type Utility Owner
Visible Marks No
Root Cause Category Locating Issue
Root Cause Type Facility Marked Inaccurately Due To Locator Error
Preparer Name W*** S******
Preparer Title Pipeline Technical Specialist
Preparer Email W***********@k***********.com
Preparer Telephone 661-304-6971
Prepared Date 2019-01-30 00:00:00
Authorizer Name Q****** F******
Authorizer Telephone 770-751-4240
Authorizer Title Director Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative At 11:20 a.M. On 11/2/2018, a 3rd party contractor called the rocklin control room reporting they had just struck a pipeline with an auger while conducting geotechnical surveys along the railroad right of way. It was determined that ls-48 had been struck and diesel was released from the line as the static pressure in the line dropped from 70 psi to 0. The line was excavated, purged, and the damaged portion cut out and replaced with a new piece. After successful static and running tests, the line was returned to normal service and remediation activities continued for several weeks afterward until the majority of the contaminated soil had been removed to the extent practicable. An investigation into the accident revealed that ls-48 did not have proper markings at the time of the initial locate or at the time of the incident, however, the parallel sfpp ls-20 was properly marked. 1/30/2019 update- no edits or additions from original. Final supplemental submitted.

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