HL incident on 2018-11-02 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2018-11-02 09:15
Report number
Location
TX
Narrative
(updated 02-14-2019) on 11/02/18 at approximately 09:15 am local pipeline technician while performing station rounds at the midland facility identified a 30 gallon (0.7bbl) release of crude oil product from the sump. � a body bleed valve on the incoming mov was found to be cracked open which contributed to the overfill of the sump tank. The pipeline technician closed the valve and the sump was emptied.� � � after investigation it was discovered that a high level alarm was not present on the sump tank affecting the ability to manage the sump tanks volume.� � operations is assessing the current sump tank for the addition of high level alarm indicator. Other locations where high level indication is not currently installed will be assessed and evaluated.
Detailed record list
Report Received Date
2018-11-30 00:00:00
Iyear
2018
Report Number
20180369
Supplemental Number
31658
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-11-02 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.7
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-11-02 09:15:00
System Part Involved
Onshore Equipment And Piping Associated With Belowground Storage
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Closed And Flow Stopped Flowing Into Sump. Facility Was Never Shutdown
On Site Datetime
2018-11-02 09:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland Station
Segment Name
Sump Tank
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Designated Name
Sump Tk 0003
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
500
Est Cost Emergency
0
Est Cost Environmental
3000
Est Cost Other
0
Prpty
3560
Accident Psig
50
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room nor controller were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Inadequate Monitoring
Related Other Ind
Yes
Operation Related Details
After Investigation It Was Discovered That A High Level Alarm Was Not Present On The Sump Tank Affecting The Ability To Indicate The Sump Tanks Volume.
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
M****** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
M*******@e****.com
Preparer Telephone
713-381-6869
Prepared Date
2019-02-14 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Compliance Manager
Authorizer Email
S******@e****.com
Narrative
(updated 02-14-2019) on 11/02/18 at approximately 09:15 am local pipeline technician while performing station rounds at the midland facility identified a 30 gallon (0.7bbl) release of crude oil product from the sump. � a body bleed valve on the incoming mov was found to be cracked open which contributed to the overfill of the sump tank. The pipeline technician closed the valve and the sump was emptied.� � � after investigation it was discovered that a high level alarm was not present on the sump tank affecting the ability to manage the sump tanks volume.� � operations is assessing the current sump tank for the addition of high level alarm indicator. Other locations where high level indication is not currently installed will be assessed and evaluated.
Report Received Date 2018-11-30 00:00:00
Iyear 2018
Report Number 20180369
Supplemental Number 31658
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-11-02 09:15:00
Location Latitude 32.023762 Google Maps OpenStreetMap
Location Longitude -102.017753 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.7
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-11-02 09:15:00
System Part Involved Onshore Equipment And Piping Associated With Belowground Storage
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Closed And Flow Stopped Flowing Into Sump. Facility Was Never Shutdown
On Site Datetime 2018-11-02 09:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Midland Station
Segment Name Sump Tank
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Midland
Onshore County Name Midland
Designated Location Milepost/valve Station
Designated Name Sump Tk 0003
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 500
Est Cost Emergency 0
Est Cost Environmental 3000
Est Cost Other 0
Prpty 3560
Accident Psig 50
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room nor controller were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Inadequate Monitoring
Related Other Ind Yes
Operation Related Details After Investigation It Was Discovered That A High Level Alarm Was Not Present On The Sump Tank Affecting The Ability To Indicate The Sump Tanks Volume.
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name M****** B*****
Preparer Title Pipeline Compliance Engineer
Preparer Email M*******@e****.com
Preparer Telephone 713-381-6869
Prepared Date 2019-02-14 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Compliance Manager
Authorizer Email S******@e****.com
Narrative (updated 02-14-2019) on 11/02/18 at approximately 09:15 am local pipeline technician while performing station rounds at the midland facility identified a 30 gallon (0.7bbl) release of crude oil product from the sump. � a body bleed valve on the incoming mov was found to be cracked open which contributed to the overfill of the sump tank. The pipeline technician closed the valve and the sump was emptied.� � � after investigation it was discovered that a high level alarm was not present on the sump tank affecting the ability to manage the sump tanks volume.� � operations is assessing the current sump tank for the addition of high level alarm indicator. Other locations where high level indication is not currently installed will be assessed and evaluated.

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