HL incident on 2018-10-26 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$19,700
Incident datetime
2018-10-26 14:43
Report number
Location
TX
Narrative
On 10/26/2018 at 14:43, pipeline control received a gas detection alarm on pump 602 at intermediate pump station (ips). Personnel arrived at the ips station at 14:48 and discovered vapors leaking from the valve stem packing tattletale. Flow was routed, valve blocked in, and de-pressured to portable flare. The valve was removed and replaced with a new valve. The valve was inspected by a 3rd party and identified the o-ring failed due to ball valve bearing being loose as well as a build up of solids in valve body.
Detailed record list
Report Received Date
2018-11-20 00:00:00
Iyear
2018
Report Number
20180362
Supplemental Number
31213
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-10-26 14:43:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
1
Intentional Release Bbls
5
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2018-10-26 14:43:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Rerouted To Isolate Leaking Valve And Continued To Flow.
On Site Datetime
2018-10-26 14:48:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Intermediate Pump Station
Segment Name
32400
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Not Within A Municipality
Onshore County Name
Harris
Designated Location
Survey Station No.
Designated Name
255+80
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Viton
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
19700
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
19800
Accident Psig
818
Mop Psig
1290
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Gas detection device at pump station caused gas detector alarm in the control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Loose Valve Bearing And Build Up Of Solids In Valve Body
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Prepared Date
2018-11-20 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Manager Compliance
Authorizer Email
N*******@e****.com
Narrative
On 10/26/2018 at 14:43, pipeline control received a gas detection alarm on pump 602 at intermediate pump station (ips). Personnel arrived at the ips station at 14:48 and discovered vapors leaking from the valve stem packing tattletale. Flow was routed, valve blocked in, and de-pressured to portable flare. The valve was removed and replaced with a new valve. The valve was inspected by a 3rd party and identified the o-ring failed due to ball valve bearing being loose as well as a build up of solids in valve body.
Report Received Date 2018-11-20 00:00:00
Iyear 2018
Report Number 20180362
Supplemental Number 31213
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-10-26 14:43:00
Location Latitude 29.720703 Google Maps OpenStreetMap
Location Longitude -95.158692 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 1
Intentional Release Bbls 5
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2018-10-26 14:43:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Rerouted To Isolate Leaking Valve And Continued To Flow.
On Site Datetime 2018-10-26 14:48:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Intermediate Pump Station
Segment Name 32400
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Not Within A Municipality
Onshore County Name Harris
Designated Location Survey Station No.
Designated Name 255+80
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Viton
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 19700
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 19800
Accident Psig 818
Mop Psig 1290
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Gas detection device at pump station caused gas detector alarm in the control room.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Loose Valve Bearing And Build Up Of Solids In Valve Body
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Prepared Date 2018-11-20 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Manager Compliance
Authorizer Email N*******@e****.com
Narrative On 10/26/2018 at 14:43, pipeline control received a gas detection alarm on pump 602 at intermediate pump station (ips). Personnel arrived at the ips station at 14:48 and discovered vapors leaking from the valve stem packing tattletale. Flow was routed, valve blocked in, and de-pressured to portable flare. The valve was removed and replaced with a new valve. The valve was inspected by a 3rd party and identified the o-ring failed due to ball valve bearing being loose as well as a build up of solids in valve body.

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