HL incident on 2018-10-19 — OK

Operator
Great Salt Plains Pipeline Llc
Cause
Excavation Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50,000
Incident datetime
2018-10-19 07:15
Report number
Location
OK
Narrative
4" hennessey pipeline spill incident report. On october 17, 2018 gspp initiated line fill on our 4" hennessey pipeline that runs from a truck injection station near hennessey oklahoma to an interconnect on the gspp 8" mainline near covington ok. Gspp personnel shutdown at 5pm. Flow was reinitiated at 8:00am on 10/18/18 to finish the line fill. On october 19, 2018, at 6:15 pm, we received a notification from orr construction that our 4 inch pipeline was leaking. The control room was notified and the pipeline pumps at our hennessey truck station were shut down. Field operations personnel were then called out to isolate the section of the line that was leaking and begin to assess the extent of the damage. The line was isolated within 1-hour of initial notification. A temporary clamp was installed over the leaking segment of pipe. Initial remediation efforts focused on extent of the contaminated water and soil and containment through use of temporary berms and installation of earthen dams. On october 20, 2018 soil and water remediation efforts commenced in earnest. Concurrently with remediation efforts, the damaged portion of the line was replaced. An inline inspection was conducted on the line to ensure that no additional damage occurred, and the line was re-hydro tested to establish maop. As of november 8, 2018 remediation efforts are ongoing and the pipeline has been returned to service. Great salt plains midstream is continuing to work with environmental engineers and the oklahoma corporation commission through the remediation process. It is estimated that 1,562 bbls have been lost and approximately 1,300 bbls have been recovered from the soil. 320 bbls have been recovered and returned to gspm pipelines. A careful review of the pipeline segment that has been placed we believe the leak is the result of an unreported line strike which had to of occurred between the time of the operational hydro test to verify line integrity and the introduction of crude oil into the pipeline. At this time we have been unable to prove who struck the pipeline and we will continue to investigate. We reviewed the one call activity for the area of the leak. All tickets were marked properly. We feel that the cga root cause is "excavation practices are not sufficient" due to the fact the line was struck without proper one call notification and post damage operator notification. Repair and remediation costs incurred at this time are still being accounted, but currently is less than $1mm. We expect to have full remediation efforts complete and full accounting of costs completed by november 30th.
Detailed record list
Report Received Date
2018-11-16 00:00:00
Iyear
2018
Report Number
20180353
Supplemental Number
31378
Report Type
Supplemental Final
Operator Id
Name
Great Salt Plains Pipeline Llc
Operator Street Address
17182 County Road 610
Operator City Name
Cherokee
Operator State Abbreviation
OK
Operator Postal Code
73728
Local Datetime
2018-10-18 11:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1567
Recovered Bbls
1300
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Noticed Oil On The Gound.
Incident Identified Datetime
2018-10-19 07:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-19 06:15:00
Restart Datetime
2018-11-09 08:55:00
On Site Datetime
2018-10-19 08:00:00
Nrc Rpt Datetime
2018-10-19 08:20:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Gspp 2
Segment Name
Gspp 2
Onshore State Abbreviation
Ok
Onshore Postal Code
73733
Onshore City Name
Douglas
Onshore County Name
Garfield
Designated Location
Milepost/valve Station
Designated Name
Balon Ball 4"
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4
Pipe Wall Thickness
0.188
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Seamless
Pipe Coating Type
Coal Tar
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
0.2
Puncture Circum
12
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
1562
Rel Water Name
Farm Pond
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
10000
Est Cost Gas Released
150000
Est Cost Prop Damage
50000
Est Cost Emergency
350000
Est Cost Environmental
400000
Est Cost Other
0
Prpty
960000
Accident Psig
1
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
26400
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Unknown/other
Excavator Equipment
Unknown/other
Work Performed
Unknown/other
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
504
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
A*** C*****
Preparer Title
Corporate Compliance Manager
Preparer Email
A******@m**********.com
Preparer Telephone
620-886-0082
Prepared Date
2018-12-19 00:00:00
Authorizer Name
A*** C*****
Authorizer Telephone
620-886-0082
Authorizer Title
Corporate Compliance Manager
Authorizer Email
A******@m**********.com
Narrative
4" hennessey pipeline spill incident report. On october 17, 2018 gspp initiated line fill on our 4" hennessey pipeline that runs from a truck injection station near hennessey oklahoma to an interconnect on the gspp 8" mainline near covington ok. Gspp personnel shutdown at 5pm. Flow was reinitiated at 8:00am on 10/18/18 to finish the line fill. On october 19, 2018, at 6:15 pm, we received a notification from orr construction that our 4 inch pipeline was leaking. The control room was notified and the pipeline pumps at our hennessey truck station were shut down. Field operations personnel were then called out to isolate the section of the line that was leaking and begin to assess the extent of the damage. The line was isolated within 1-hour of initial notification. A temporary clamp was installed over the leaking segment of pipe. Initial remediation efforts focused on extent of the contaminated water and soil and containment through use of temporary berms and installation of earthen dams. On october 20, 2018 soil and water remediation efforts commenced in earnest. Concurrently with remediation efforts, the damaged portion of the line was replaced. An inline inspection was conducted on the line to ensure that no additional damage occurred, and the line was re-hydro tested to establish maop. As of november 8, 2018 remediation efforts are ongoing and the pipeline has been returned to service. Great salt plains midstream is continuing to work with environmental engineers and the oklahoma corporation commission through the remediation process. It is estimated that 1,562 bbls have been lost and approximately 1,300 bbls have been recovered from the soil. 320 bbls have been recovered and returned to gspm pipelines. A careful review of the pipeline segment that has been placed we believe the leak is the result of an unreported line strike which had to of occurred between the time of the operational hydro test to verify line integrity and the introduction of crude oil into the pipeline. At this time we have been unable to prove who struck the pipeline and we will continue to investigate. We reviewed the one call activity for the area of the leak. All tickets were marked properly. We feel that the cga root cause is "excavation practices are not sufficient" due to the fact the line was struck without proper one call notification and post damage operator notification. Repair and remediation costs incurred at this time are still being accounted, but currently is less than $1mm. We expect to have full remediation efforts complete and full accounting of costs completed by november 30th.
Report Received Date 2018-11-16 00:00:00
Iyear 2018
Report Number 20180353
Supplemental Number 31378
Report Type Supplemental Final
Operator Id 39401 PHMSA Enforcement
Name Great Salt Plains Pipeline Llc
Operator Street Address 17182 County Road 610
Operator City Name Cherokee
Operator State Abbreviation OK
Operator Postal Code 73728
Local Datetime 2018-10-18 11:00:00
Location Latitude 36.240353 Google Maps OpenStreetMap
Location Longitude -97.710377 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1567
Recovered Bbls 1300
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Noticed Oil On The Gound.
Incident Identified Datetime 2018-10-19 07:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-19 06:15:00
Restart Datetime 2018-11-09 08:55:00
On Site Datetime 2018-10-19 08:00:00
Nrc Rpt Datetime 2018-10-19 08:20:00
Nrc Rpt Num 1227991 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Gspp 2
Segment Name Gspp 2
Onshore State Abbreviation Ok
Onshore Postal Code 73733
Onshore City Name Douglas
Onshore County Name Garfield
Designated Location Milepost/valve Station
Designated Name Balon Ball 4"
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4
Pipe Wall Thickness 0.188
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Seamless
Pipe Coating Type Coal Tar
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 0.2
Puncture Circum 12
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 1562
Rel Water Name Farm Pond
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 10000
Est Cost Gas Released 150000
Est Cost Prop Damage 50000
Est Cost Emergency 350000
Est Cost Environmental 400000
Est Cost Other 0
Prpty 960000
Accident Psig 1
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 26400
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Unknown/other
Excavator Equipment Unknown/other
Work Performed Unknown/other
One Call Notified Ind No
Service Interruption Yes
Service Interruption Hours 504
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name A*** C*****
Preparer Title Corporate Compliance Manager
Preparer Email A******@m**********.com
Preparer Telephone 620-886-0082
Prepared Date 2018-12-19 00:00:00
Authorizer Name A*** C*****
Authorizer Telephone 620-886-0082
Authorizer Title Corporate Compliance Manager
Authorizer Email A******@m**********.com
Narrative 4" hennessey pipeline spill incident report. On october 17, 2018 gspp initiated line fill on our 4" hennessey pipeline that runs from a truck injection station near hennessey oklahoma to an interconnect on the gspp 8" mainline near covington ok. Gspp personnel shutdown at 5pm. Flow was reinitiated at 8:00am on 10/18/18 to finish the line fill. On october 19, 2018, at 6:15 pm, we received a notification from orr construction that our 4 inch pipeline was leaking. The control room was notified and the pipeline pumps at our hennessey truck station were shut down. Field operations personnel were then called out to isolate the section of the line that was leaking and begin to assess the extent of the damage. The line was isolated within 1-hour of initial notification. A temporary clamp was installed over the leaking segment of pipe. Initial remediation efforts focused on extent of the contaminated water and soil and containment through use of temporary berms and installation of earthen dams. On october 20, 2018 soil and water remediation efforts commenced in earnest. Concurrently with remediation efforts, the damaged portion of the line was replaced. An inline inspection was conducted on the line to ensure that no additional damage occurred, and the line was re-hydro tested to establish maop. As of november 8, 2018 remediation efforts are ongoing and the pipeline has been returned to service. Great salt plains midstream is continuing to work with environmental engineers and the oklahoma corporation commission through the remediation process. It is estimated that 1,562 bbls have been lost and approximately 1,300 bbls have been recovered from the soil. 320 bbls have been recovered and returned to gspm pipelines. A careful review of the pipeline segment that has been placed we believe the leak is the result of an unreported line strike which had to of occurred between the time of the operational hydro test to verify line integrity and the introduction of crude oil into the pipeline. At this time we have been unable to prove who struck the pipeline and we will continue to investigate. We reviewed the one call activity for the area of the leak. All tickets were marked properly. We feel that the cga root cause is "excavation practices are not sufficient" due to the fact the line was struck without proper one call notification and post damage operator notification. Repair and remediation costs incurred at this time are still being accounted, but currently is less than $1mm. We expect to have full remediation efforts complete and full accounting of costs completed by november 30th.

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