Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2018-10-26 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,500
Incident datetime
2018-10-26 14:33
Report number
Location
TX
Narrative
Third party operator notified cushing/buxton facility of crude discovered on the surface of the ground between cushing and buxton stations. Pipeline operations excavated and discovered a pin hole leak on the bend of the 12inch inner transfer line from the lact units to the cushing station tanks. Segment was removed and sent to lab for metallurgical analysis. Line was repaired and placed back into service on 10/31/2018 2019-1-8 - updated part g, item 8. Results determined based on metallurgical analysis.
Detailed record list
Report Received Date
2018-11-16 00:00:00
Iyear
2018
Report Number
20180352
Supplemental Number
31447
Report Type
Supplemental Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2018-10-26 14:33:00
Location Latitude
35.947101
Location Longitude
-96.753007
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.9
Recovered Bbls
2.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Local Third Party Operator
Incident Identified Datetime
2018-10-26 14:33:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-26 14:55:00
Restart Datetime
2018-10-31 09:30:00
On Site Datetime
2018-10-26 15:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Terminal
Segment Name
Facility Transfer Piping
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cushing Termi
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
50
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Ml Lilley
Pipe Coating Type
Cold Applied Tape
Installation Year
1999
Manufactured Year
1999
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
1500
Est Cost Emergency
25000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
31700
Accident Psig
85
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak rate and size was not detectable by controller or control room
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2014
Hydrtst Most Rcnt Pressure
400
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J*** B*********
Preparer Title
Dot Coordinator
Preparer Email
J**************@p**.com
Preparer Telephone
580-767-4206
Prepared Date
2019-01-08 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director, Dot Compliance
Authorizer Email
T***********@p**.com
Narrative
Third party operator notified cushing/buxton facility of crude discovered on the surface of the ground between cushing and buxton stations. Pipeline operations excavated and discovered a pin hole leak on the bend of the 12inch inner transfer line from the lact units to the cushing station tanks. Segment was removed and sent to lab for metallurgical analysis. Line was repaired and placed back into service on 10/31/2018 2019-1-8 - updated part g, item 8. Results determined based on metallurgical analysis.
| Report Received Date | 2018-11-16 00:00:00 |
|---|---|
| Iyear | 2018 |
| Report Number | 20180352 |
| Supplemental Number | 31447 |
| Report Type | Supplemental Final |
| Operator Id | 31684 PHMSA Enforcement |
| Name | Phillips 66 Pipeline Llc |
| Operator Street Address | 2331 Citywest Blvd |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77042 |
| Local Datetime | 2018-10-26 14:33:00 |
| Location Latitude | 35.947101 Google Maps OpenStreetMap |
| Location Longitude | -96.753007 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2.9 |
| Recovered Bbls | 2.9 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Other |
| Accident Details | Local Third Party Operator |
| Incident Identified Datetime | 2018-10-26 14:33:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2018-10-26 14:55:00 |
| Restart Datetime | 2018-10-31 09:30:00 |
| On Site Datetime | 2018-10-26 15:00:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Cushing Terminal |
| Segment Name | Facility Transfer Piping |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74023 |
| Onshore City Name | Cushing |
| Onshore County Name | Payne |
| Designated Location | Milepost/valve Station |
| Designated Name | Cushing Termi |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 50 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 12 |
| Pipe Wall Thickness | 0.25 |
| Pipe Smys | 52000 |
| Pipe Specification | Api 5l |
| Pipe Seam Type | Erw - Low Frequency |
| Pipe Manufacturer | Ml Lilley |
| Pipe Coating Type | Cold Applied Tape |
| Installation Year | 1999 |
| Manufactured Year | 1999 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 200 |
| Est Cost Prop Damage | 1500 |
| Est Cost Emergency | 25000 |
| Est Cost Environmental | 5000 |
| Est Cost Other | 0 |
| Prpty | 31700 |
| Accident Psig | 85 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Leak rate and size was not detectable by controller or control room |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Localized Pitting |
| Int Water Acid Ind | Yes |
| Int Metallurgical Basis Ind | Yes |
| Int Low Point Pipe Loc Ind | Yes |
| Corrosion Inhibitors | No |
| Corrosion Lining | No |
| Cleaning Dewatering | Yes |
| Corrosion Coupons | Not Applicable - Not Mainline Pipe |
| Collected Data Ind | No |
| Has Hydrtst Conduc Before Ind | Yes |
| Hydrtst Most Rcnt Year | 2014 |
| Hydrtst Most Rcnt Pressure | 400 |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | J*** B********* |
| Preparer Title | Dot Coordinator |
| Preparer Email | J**************@p**.com |
| Preparer Telephone | 580-767-4206 |
| Prepared Date | 2019-01-08 00:00:00 |
| Authorizer Name | T*** F**** |
| Authorizer Telephone | 832-765-1632 |
| Authorizer Title | Director, Dot Compliance |
| Authorizer Email | T***********@p**.com |
| Narrative | Third party operator notified cushing/buxton facility of crude discovered on the surface of the ground between cushing and buxton stations. Pipeline operations excavated and discovered a pin hole leak on the bend of the 12inch inner transfer line from the lact units to the cushing station tanks. Segment was removed and sent to lab for metallurgical analysis. Line was repaired and placed back into service on 10/31/2018 2019-1-8 - updated part g, item 8. Results determined based on metallurgical analysis. |
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