HL incident on 2018-10-26 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2018-10-26 14:33
Report number
Location
TX
Narrative
Third party operator notified cushing/buxton facility of crude discovered on the surface of the ground between cushing and buxton stations. Pipeline operations excavated and discovered a pin hole leak on the bend of the 12inch inner transfer line from the lact units to the cushing station tanks. Segment was removed and sent to lab for metallurgical analysis. Line was repaired and placed back into service on 10/31/2018 2019-1-8 - updated part g, item 8. Results determined based on metallurgical analysis.
Detailed record list
Report Received Date
2018-11-16 00:00:00
Iyear
2018
Report Number
20180352
Supplemental Number
31447
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2018-10-26 14:33:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.9
Recovered Bbls
2.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Local Third Party Operator
Incident Identified Datetime
2018-10-26 14:33:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-26 14:55:00
Restart Datetime
2018-10-31 09:30:00
On Site Datetime
2018-10-26 15:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Terminal
Segment Name
Facility Transfer Piping
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cushing Termi
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
50
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Ml Lilley
Pipe Coating Type
Cold Applied Tape
Installation Year
1999
Manufactured Year
1999
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
1500
Est Cost Emergency
25000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
31700
Accident Psig
85
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak rate and size was not detectable by controller or control room
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2014
Hydrtst Most Rcnt Pressure
400
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J*** B*********
Preparer Title
Dot Coordinator
Preparer Email
J**************@p**.com
Preparer Telephone
580-767-4206
Prepared Date
2019-01-08 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director, Dot Compliance
Authorizer Email
T***********@p**.com
Narrative
Third party operator notified cushing/buxton facility of crude discovered on the surface of the ground between cushing and buxton stations. Pipeline operations excavated and discovered a pin hole leak on the bend of the 12inch inner transfer line from the lact units to the cushing station tanks. Segment was removed and sent to lab for metallurgical analysis. Line was repaired and placed back into service on 10/31/2018 2019-1-8 - updated part g, item 8. Results determined based on metallurgical analysis.
Report Received Date 2018-11-16 00:00:00
Iyear 2018
Report Number 20180352
Supplemental Number 31447
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2018-10-26 14:33:00
Location Latitude 35.947101 Google Maps OpenStreetMap
Location Longitude -96.753007 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2.9
Recovered Bbls 2.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Local Third Party Operator
Incident Identified Datetime 2018-10-26 14:33:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-26 14:55:00
Restart Datetime 2018-10-31 09:30:00
On Site Datetime 2018-10-26 15:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing Terminal
Segment Name Facility Transfer Piping
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Cushing Termi
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 50
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Ml Lilley
Pipe Coating Type Cold Applied Tape
Installation Year 1999
Manufactured Year 1999
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 1500
Est Cost Emergency 25000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 31700
Accident Psig 85
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak rate and size was not detectable by controller or control room
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2014
Hydrtst Most Rcnt Pressure 400
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J*** B*********
Preparer Title Dot Coordinator
Preparer Email J**************@p**.com
Preparer Telephone 580-767-4206
Prepared Date 2019-01-08 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Director, Dot Compliance
Authorizer Email T***********@p**.com
Narrative Third party operator notified cushing/buxton facility of crude discovered on the surface of the ground between cushing and buxton stations. Pipeline operations excavated and discovered a pin hole leak on the bend of the 12inch inner transfer line from the lact units to the cushing station tanks. Segment was removed and sent to lab for metallurgical analysis. Line was repaired and placed back into service on 10/31/2018 2019-1-8 - updated part g, item 8. Results determined based on metallurgical analysis.

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