HL incident on 2018-10-18 — OK

Operator
Explorer Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25
Incident datetime
2018-10-18 09:34
Report number
Location
OK
Narrative
On october 18, 2018 an explorer pipeline technician identified a release of diesel fuel from a ferrule fitting associated with 0.75 inch tubing on a preview gravitometer. The technician immediately isolated the gravitometer from the pipeline, and notified the control center that the device was isolated from the pipeline. The release was totally contained inside the fenced gravitometer station, and any impacted soil and gravel was properly tested and managed. The initial response measurements and calculations reflected that the release would be under the reportable quantity. However, laboratory results from the soil reflected that the total amount of diesel fuel in the soil was over 5.00 gallons. The actual release volume was 7.50 gallons.
Detailed record list
Report Received Date
2018-11-15 00:00:00
Iyear
2018
Report Number
20180349
Supplemental Number
32012
Report Type
Supplemental Final
Operator Id
Name
Explorer Pipeline Co
Operator Street Address
Po Box 2650
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74101
Local Datetime
2018-10-18 09:34:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-10-18 09:34:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Gravitometer Could Be Isolated From The Pipeline.
On Site Datetime
2018-10-18 09:34:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
East Saint Louis Preview Gravitometer
Segment Name
Wood River Tank Farm To East St. Louis Station
Onshore State Abbreviation
Il
Onshore Postal Code
62206
Onshore City Name
Sauget
Onshore County Name
Saint Clair
Designated Location
Milepost/valve Station
Designated Name
18.18
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2018
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Stell
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
12
Est Cost Prop Damage
25
Est Cost Emergency
500
Est Cost Environmental
3500
Est Cost Other
0
Prpty
4037
Accident Psig
230
Mop Psig
1337
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
The Asset Involved With The 7.5 Gallon Release Was Tubing For A Remote Gravitometer Off The Pipeline, Not The Pipeline.
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release from gravitometer tubing was not caused or contributed by the actions or inactions of the pipeline controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Installation Ind
Yes
Preparer Name
K**** E* B****
Preparer Title
Manager Dot Compliance
Preparer Email
K*****@e***.com
Preparer Telephone
9184935104
Prepared Date
2019-04-24 00:00:00
Authorizer Name
J** S****
Authorizer Telephone
9184935143
Authorizer Title
Director Engineering And Hsse
Authorizer Email
J*****@e***.com
Narrative
On october 18, 2018 an explorer pipeline technician identified a release of diesel fuel from a ferrule fitting associated with 0.75 inch tubing on a preview gravitometer. The technician immediately isolated the gravitometer from the pipeline, and notified the control center that the device was isolated from the pipeline. The release was totally contained inside the fenced gravitometer station, and any impacted soil and gravel was properly tested and managed. The initial response measurements and calculations reflected that the release would be under the reportable quantity. However, laboratory results from the soil reflected that the total amount of diesel fuel in the soil was over 5.00 gallons. The actual release volume was 7.50 gallons.
Report Received Date 2018-11-15 00:00:00
Iyear 2018
Report Number 20180349
Supplemental Number 32012
Report Type Supplemental Final
Operator Id 4805 PHMSA Enforcement
Name Explorer Pipeline Co
Operator Street Address Po Box 2650
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74101
Local Datetime 2018-10-18 09:34:00
Location Latitude 38.602775 Google Maps OpenStreetMap
Location Longitude -90.179371 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-10-18 09:34:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Gravitometer Could Be Isolated From The Pipeline.
On Site Datetime 2018-10-18 09:34:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name East Saint Louis Preview Gravitometer
Segment Name Wood River Tank Farm To East St. Louis Station
Onshore State Abbreviation Il
Onshore Postal Code 62206
Onshore City Name Sauget
Onshore County Name Saint Clair
Designated Location Milepost/valve Station
Designated Name 18.18
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2018
Material Involved Material Other Than Carbon Steel
Material Details Stainless Stell
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 12
Est Cost Prop Damage 25
Est Cost Emergency 500
Est Cost Environmental 3500
Est Cost Other 0
Prpty 4037
Accident Psig 230
Mop Psig 1337
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details The Asset Involved With The 7.5 Gallon Release Was Tubing For A Remote Gravitometer Off The Pipeline, Not The Pipeline.
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release from gravitometer tubing was not caused or contributed by the actions or inactions of the pipeline controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Installation Ind Yes
Preparer Name K**** E* B****
Preparer Title Manager Dot Compliance
Preparer Email K*****@e***.com
Preparer Telephone 9184935104
Prepared Date 2019-04-24 00:00:00
Authorizer Name J** S****
Authorizer Telephone 9184935143
Authorizer Title Director Engineering And Hsse
Authorizer Email J*****@e***.com
Narrative On october 18, 2018 an explorer pipeline technician identified a release of diesel fuel from a ferrule fitting associated with 0.75 inch tubing on a preview gravitometer. The technician immediately isolated the gravitometer from the pipeline, and notified the control center that the device was isolated from the pipeline. The release was totally contained inside the fenced gravitometer station, and any impacted soil and gravel was properly tested and managed. The initial response measurements and calculations reflected that the release would be under the reportable quantity. However, laboratory results from the soil reflected that the total amount of diesel fuel in the soil was over 5.00 gallons. The actual release volume was 7.50 gallons.

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