HL incident on 2018-10-18 — LA

Operator
Crimson Gulf, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2018-10-18 07:10
Report number
Location
LA
Narrative
Operator making morning rounds discovered crude oil on concrete pad at the meter skid. Less than 1 gallon of crude was released and pushed over deck by wind into the mud/marsh area below. The cause was due to a packing seal leak on a flow control valve. The operator replacement the seal packing plate to stop/secure the release. Operator cleaned and secured the release area using absorbent materials.
Detailed record list
Report Received Date
2018-11-13 00:00:00
Iyear
2018
Report Number
20180348
Supplemental Number
31789
Report Type
Supplemental Final
Operator Id
Name
Crimson Gulf, Llc
Operator Street Address
263 Trinity Lane
Operator City Name
Gray
Operator State Abbreviation
LA
Operator Postal Code
70359
Local Datetime
2018-10-18 07:10:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-10-18 07:10:00
System Part Involved
Offshore Platform/deepwater Port, Including Platform-Mounted Equipment And Piping
On Off Shore
Offshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-18 07:10:00
Restart Datetime
2018-10-18 08:15:00
On Site Datetime
2018-10-18 07:10:00
Nrc Rpt Datetime
2018-10-18 07:31:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Off Water Depth
5
Off Accident Origin
In State Waters
Offshore State Abbreviation
La
Off Instate Area
Facility
Off Instate Block
Main Pass 72
Offshore County Name
Plaquemines
Off Area Accident Type
Platform
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
0.02
Rel Water Name
Gom Inlet
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
100
Est Cost Emergency
100
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Operator On Site Tightened Flange Fitting.
Prpty
200
Accident Psig
184
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Seepage from a gasket would not have been detected by controller. Release was identified by a operator making daily rounds of the facility.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Control Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Gasket Fatigue On Flow Control Valve
Preparer Name
D**** B********
Preparer Title
Regulatory Compliance Manager
Preparer Email
D*********@c********.com
Preparer Telephone
5626680066
Preparer Fax
5622854141
Prepared Date
2019-03-14 00:00:00
Authorizer Name
L**** W* A********
Authorizer Telephone
5622854100
Authorizer Title
President
Authorizer Email
L**********@c********.com
Narrative
Operator making morning rounds discovered crude oil on concrete pad at the meter skid. Less than 1 gallon of crude was released and pushed over deck by wind into the mud/marsh area below. The cause was due to a packing seal leak on a flow control valve. The operator replacement the seal packing plate to stop/secure the release. Operator cleaned and secured the release area using absorbent materials.
Report Received Date 2018-11-13 00:00:00
Iyear 2018
Report Number 20180348
Supplemental Number 31789
Report Type Supplemental Final
Operator Id 39084 PHMSA Enforcement
Name Crimson Gulf, Llc
Operator Street Address 263 Trinity Lane
Operator City Name Gray
Operator State Abbreviation LA
Operator Postal Code 70359
Local Datetime 2018-10-18 07:10:00
Location Latitude 29.203019 Google Maps OpenStreetMap
Location Longitude -89.04394 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-10-18 07:10:00
System Part Involved Offshore Platform/deepwater Port, Including Platform-Mounted Equipment And Piping
On Off Shore Offshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-18 07:10:00
Restart Datetime 2018-10-18 08:15:00
On Site Datetime 2018-10-18 07:10:00
Nrc Rpt Datetime 2018-10-18 07:31:00
Nrc Rpt Num 1227797 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Off Water Depth 5
Off Accident Origin In State Waters
Offshore State Abbreviation La
Off Instate Area Facility
Off Instate Block Main Pass 72
Offshore County Name Plaquemines
Off Area Accident Type Platform
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Ocean Seawater Ind Yes
Amount Released 0.02
Rel Water Name Gom Inlet
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 100
Est Cost Emergency 100
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Operator On Site Tightened Flange Fitting.
Prpty 200
Accident Psig 184
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Seepage from a gasket would not have been detected by controller. Release was identified by a operator making daily rounds of the facility.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Control Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Gasket Fatigue On Flow Control Valve
Preparer Name D**** B********
Preparer Title Regulatory Compliance Manager
Preparer Email D*********@c********.com
Preparer Telephone 5626680066
Preparer Fax 5622854141
Prepared Date 2019-03-14 00:00:00
Authorizer Name L**** W* A********
Authorizer Telephone 5622854100
Authorizer Title President
Authorizer Email L**********@c********.com
Narrative Operator making morning rounds discovered crude oil on concrete pad at the meter skid. Less than 1 gallon of crude was released and pushed over deck by wind into the mud/marsh area below. The cause was due to a packing seal leak on a flow control valve. The operator replacement the seal packing plate to stop/secure the release. Operator cleaned and secured the release area using absorbent materials.

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