HL incident on 2018-10-08 — TX

Operator
Kinder Morgan Co2 Co. Lp
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$92,970
Incident datetime
2018-10-08 12:45
Report number
Location
TX
Narrative
On 10/8/2018, a kinder morgan employee discovered CO2/ice at crc, mlv 12. The ice was coming up from the valve, underground. Co2 was not blowing to the atmosphere. The valve was hydro excavated and stem packing replaced. It was determined that the o-ring failed based on a visual inspection. The o-ring lost mechanical properties and severed. The following is a continuation from part a, question #6: a 48-hour follow up to the nrc was on 10/09/2018 at 14:13 cst, report # 1226992. An additional update was made to the nrc on 10/10/2018 at 9:05 cst, report # 1227073. The following is a continuation from part a, questions 14a & 14b: crc pipeline was shut-in a second time on 10/10/2018 at 08:51 cst. Crc pipeline was restarted on 10/11/2018 at 08:21 cst.
Detailed record list
Report Received Date
2018-11-06 00:00:00
Iyear
2018
Report Number
20180339
Supplemental Number
31467
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Co2 Co. Lp
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-10-08 12:45:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
7.3
Intentional Release Bbls
29140
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-10-08 12:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-09 08:31:00
Restart Datetime
2018-10-09 11:49:00
On Site Datetime
2018-10-08 12:45:00
Nrc Rpt Datetime
2018-10-08 13:39:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Crc Pipeline
Segment Name
Mlv 12
Onshore State Abbreviation
Tx
Onshore Postal Code
79752
Onshore City Name
Rankin
Onshore County Name
Upton
Designated Location
Milepost/valve Station
Designated Name
12
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Ball
Valve Manufacturer
Cameron
Installation Year
2003
Manufactured Year
2003
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
19
Est Cost Prop Damage
92970
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
92989
Accident Psig
1500
Mop Psig
2025
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
126720
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The affected valve is not invisible in scada. Based on the minimal amount of volume lost, the leak was undetectable by the control center. Local field operations notified the control center of the leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Breakdown Ind
Yes
Preparer Name
A**** Z*****
Preparer Title
Manager-Regulatory Compliance
Preparer Email
A***********@k***********.com
Preparer Telephone
713-369-9512
Preparer Fax
303-984-3417
Prepared Date
2019-01-10 00:00:00
Authorizer Name
M***** L*******
Authorizer Telephone
713-420-4649
Authorizer Title
Director-Operations And Engineering
Authorizer Email
M**************@k***********.com
Narrative
On 10/8/2018, a kinder morgan employee discovered CO2/ice at crc, mlv 12. The ice was coming up from the valve, underground. Co2 was not blowing to the atmosphere. The valve was hydro excavated and stem packing replaced. It was determined that the o-ring failed based on a visual inspection. The o-ring lost mechanical properties and severed. The following is a continuation from part a, question #6: a 48-hour follow up to the nrc was on 10/09/2018 at 14:13 cst, report # 1226992. An additional update was made to the nrc on 10/10/2018 at 9:05 cst, report # 1227073. The following is a continuation from part a, questions 14a & 14b: crc pipeline was shut-in a second time on 10/10/2018 at 08:51 cst. Crc pipeline was restarted on 10/11/2018 at 08:21 cst.
Report Received Date 2018-11-06 00:00:00
Iyear 2018
Report Number 20180339
Supplemental Number 31467
Report Type Supplemental Final
Operator Id 31555 PHMSA Enforcement
Name Kinder Morgan Co2 Co. Lp
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-10-08 12:45:00
Location Latitude 31.408075 Google Maps OpenStreetMap
Location Longitude -102.081016 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 7.3
Intentional Release Bbls 29140
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-10-08 12:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-09 08:31:00
Restart Datetime 2018-10-09 11:49:00
On Site Datetime 2018-10-08 12:45:00
Nrc Rpt Datetime 2018-10-08 13:39:00
Nrc Rpt Num 1226883 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Crc Pipeline
Segment Name Mlv 12
Onshore State Abbreviation Tx
Onshore Postal Code 79752
Onshore City Name Rankin
Onshore County Name Upton
Designated Location Milepost/valve Station
Designated Name 12
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Ball
Valve Manufacturer Cameron
Installation Year 2003
Manufactured Year 2003
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 19
Est Cost Prop Damage 92970
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 92989
Accident Psig 1500
Mop Psig 2025
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 126720
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The affected valve is not invisible in scada. Based on the minimal amount of volume lost, the leak was undetectable by the control center. Local field operations notified the control center of the leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Additional Breakdown Ind Yes
Preparer Name A**** Z*****
Preparer Title Manager-Regulatory Compliance
Preparer Email A***********@k***********.com
Preparer Telephone 713-369-9512
Preparer Fax 303-984-3417
Prepared Date 2019-01-10 00:00:00
Authorizer Name M***** L*******
Authorizer Telephone 713-420-4649
Authorizer Title Director-Operations And Engineering
Authorizer Email M**************@k***********.com
Narrative On 10/8/2018, a kinder morgan employee discovered CO2/ice at crc, mlv 12. The ice was coming up from the valve, underground. Co2 was not blowing to the atmosphere. The valve was hydro excavated and stem packing replaced. It was determined that the o-ring failed based on a visual inspection. The o-ring lost mechanical properties and severed. The following is a continuation from part a, question #6: a 48-hour follow up to the nrc was on 10/09/2018 at 14:13 cst, report # 1226992. An additional update was made to the nrc on 10/10/2018 at 9:05 cst, report # 1227073. The following is a continuation from part a, questions 14a & 14b: crc pipeline was shut-in a second time on 10/10/2018 at 08:51 cst. Crc pipeline was restarted on 10/11/2018 at 08:21 cst.

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