HL incident on 2018-10-11 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-10-11 17:30
Report number
Location
GA
Narrative
On october 11th at approximately 17:30, a project inspector was inspecting a compact expanding gate valve (ceg) that was recently installed on the line 01 relief system at atlanta junction. The ceg valve had been purchased in 2018 and installed on october 9th as part of a dual line relief project. The inspector noticed an odor coming from the area and upon further investigation of the area saw gasoline seeping out of the 1/2" needle vent valve located on top of the bonnet of the valve and part of the block and bleed auxiliary tubing. The 1/2" vent valve was not fully closed so the inspector tightened the hex nut on the end of the needle valve 1/4 turn which stopped the flow of product coming from the small vent port. The port on the vent valve was also plugged as a permanent repair. This type of valve is closed with a threaded hex head plug not a handle. The project inspector notified the project manager who notified the operations manager at 17:39 on october 11, 2018. This valve is attached to tank 339's tank line which was empty on october 9th when the ceg was installed. However the line was filled with product on october 11th when local operations transferred product from the gasoline sump into the tank line. There was standing water in the area from tropical storm michael which had flooded the mainfold area with approximately 6 inches of water. The product that was released was contained on the standing water and recovered using sorbent pads. All product was recovered by 19:00 on october 11th. A 16.8 gallon spill volume was calculated from the number of sorbents used to collect free product. No nrc, local, state or federal agencies were required to be notified due to not meeting any of the requirements to notify those agencies. Supplement 12/11/18 this supplement changes the cause from "other" to "equipment failure" due to a request from PHMSA.
Detailed record list
Report Received Date
2018-11-02 00:00:00
Iyear
2018
Report Number
20180338
Supplemental Number
31306
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2018-10-11 17:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.4
Recovered Bbls
0.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-10-11 17:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Needle Vent Valve Was Immediately Closed By Person That Discovered Leak.
On Site Datetime
2018-10-11 17:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Atlanta Junction
Segment Name
Line 1 Relief Line
Onshore State Abbreviation
Ga
Onshore Postal Code
30106
Onshore City Name
Austell
Onshore County Name
Cobb
Designated Location
Milepost/valve Station
Designated Name
520
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Other
Valve Mainline Details
Compact Expanding Gate Valve
Valve Manufacturer
M&j
Installation Year
2018
Manufactured Year
2018
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Other
Release Type Details
The Vent Valve For Body Block And Bleed On A New Compact Expanding Gate Valve Was Open.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
16
Est Cost Prop Damage
0
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
1016
Accident Psig
10
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Failure To Check Fitting During Installation Of New Valve.
Preparer Name
D***** L******
Preparer Title
Compliance Coordinator Sed
Preparer Email
D*******@c******.com
Preparer Telephone
443-821-1456
Prepared Date
2018-12-11 00:00:00
Authorizer Name
D***** L******
Authorizer Telephone
443-821-1456
Authorizer Title
Compliance Coordinator
Authorizer Email
D*******@c******.com
Narrative
On october 11th at approximately 17:30, a project inspector was inspecting a compact expanding gate valve (ceg) that was recently installed on the line 01 relief system at atlanta junction. The ceg valve had been purchased in 2018 and installed on october 9th as part of a dual line relief project. The inspector noticed an odor coming from the area and upon further investigation of the area saw gasoline seeping out of the 1/2" needle vent valve located on top of the bonnet of the valve and part of the block and bleed auxiliary tubing. The 1/2" vent valve was not fully closed so the inspector tightened the hex nut on the end of the needle valve 1/4 turn which stopped the flow of product coming from the small vent port. The port on the vent valve was also plugged as a permanent repair. This type of valve is closed with a threaded hex head plug not a handle. The project inspector notified the project manager who notified the operations manager at 17:39 on october 11, 2018. This valve is attached to tank 339's tank line which was empty on october 9th when the ceg was installed. However the line was filled with product on october 11th when local operations transferred product from the gasoline sump into the tank line. There was standing water in the area from tropical storm michael which had flooded the mainfold area with approximately 6 inches of water. The product that was released was contained on the standing water and recovered using sorbent pads. All product was recovered by 19:00 on october 11th. A 16.8 gallon spill volume was calculated from the number of sorbents used to collect free product. No nrc, local, state or federal agencies were required to be notified due to not meeting any of the requirements to notify those agencies. Supplement 12/11/18 this supplement changes the cause from "other" to "equipment failure" due to a request from PHMSA.
Report Received Date 2018-11-02 00:00:00
Iyear 2018
Report Number 20180338
Supplemental Number 31306
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2018-10-11 17:30:00
Location Latitude 33.85702 Google Maps OpenStreetMap
Location Longitude -84.62953 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.4
Recovered Bbls 0.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-10-11 17:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Needle Vent Valve Was Immediately Closed By Person That Discovered Leak.
On Site Datetime 2018-10-11 17:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Atlanta Junction
Segment Name Line 1 Relief Line
Onshore State Abbreviation Ga
Onshore Postal Code 30106
Onshore City Name Austell
Onshore County Name Cobb
Designated Location Milepost/valve Station
Designated Name 520
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Other
Valve Mainline Details Compact Expanding Gate Valve
Valve Manufacturer M&j
Installation Year 2018
Manufactured Year 2018
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Other
Release Type Details The Vent Valve For Body Block And Bleed On A New Compact Expanding Gate Valve Was Open.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 16
Est Cost Prop Damage 0
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 1016
Accident Psig 10
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Failure To Check Fitting During Installation Of New Valve.
Preparer Name D***** L******
Preparer Title Compliance Coordinator Sed
Preparer Email D*******@c******.com
Preparer Telephone 443-821-1456
Prepared Date 2018-12-11 00:00:00
Authorizer Name D***** L******
Authorizer Telephone 443-821-1456
Authorizer Title Compliance Coordinator
Authorizer Email D*******@c******.com
Narrative On october 11th at approximately 17:30, a project inspector was inspecting a compact expanding gate valve (ceg) that was recently installed on the line 01 relief system at atlanta junction. The ceg valve had been purchased in 2018 and installed on october 9th as part of a dual line relief project. The inspector noticed an odor coming from the area and upon further investigation of the area saw gasoline seeping out of the 1/2" needle vent valve located on top of the bonnet of the valve and part of the block and bleed auxiliary tubing. The 1/2" vent valve was not fully closed so the inspector tightened the hex nut on the end of the needle valve 1/4 turn which stopped the flow of product coming from the small vent port. The port on the vent valve was also plugged as a permanent repair. This type of valve is closed with a threaded hex head plug not a handle. The project inspector notified the project manager who notified the operations manager at 17:39 on october 11, 2018. This valve is attached to tank 339's tank line which was empty on october 9th when the ceg was installed. However the line was filled with product on october 11th when local operations transferred product from the gasoline sump into the tank line. There was standing water in the area from tropical storm michael which had flooded the mainfold area with approximately 6 inches of water. The product that was released was contained on the standing water and recovered using sorbent pads. All product was recovered by 19:00 on october 11th. A 16.8 gallon spill volume was calculated from the number of sorbents used to collect free product. No nrc, local, state or federal agencies were required to be notified due to not meeting any of the requirements to notify those agencies. Supplement 12/11/18 this supplement changes the cause from "other" to "equipment failure" due to a request from PHMSA.

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