HL incident on 2018-10-07 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2018-10-07 07:55
Report number
Location
TX
Narrative
On 10/7/2018 at 7:50 am lid 914f-100 (line 9) was lined up to deliver into tank 162. Shortly after start up, operator noticed product leaking on a 10" blind flange on tank 162. The movement was shut down immediately. It was discover that a 10" valve had a broken pin that connected the valve stem to the sealing mechanism inside the valve body. As a result, the valve indicator showed to be open but it remained 100% closed. Additionally, the pressure transmitter that monitored the line pressure had blockage in the port so it did not trigger the sdv to close, resulting in an overpressure. The overpressure caused a leak at the blind flange. No product was recovered. The 10" valve was replaced and the pressure transmitter ports were cleared of debris. Trrc was notified of the accident immediately following confirmation of volume loss exceeding the 5 gallon threshold on 10/8/2018 at 17:26hrs; trrc incident #1857
Detailed record list
Report Received Date
2018-11-02 00:00:00
Iyear
2018
Report Number
20180337
Supplemental Number
31146
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-10-07 07:55:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-10-07 07:55:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-07 07:55:00
Restart Datetime
2018-10-22 08:00:00
On Site Datetime
2018-10-07 07:55:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lid 914f-100
Segment Name
Mont Belvieu To Morgans Point #9
Onshore State Abbreviation
Tx
Onshore Postal Code
77571
Onshore City Name
Morgan's Point
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Mp 0.0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
15000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
15100
Accident Psig
790
Mop Psig
285
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Valve line up was done manual by operations - not by control room
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Additional Other Ind
Yes
Eq Additional Other Details
Pin That Connects Valve Stem To Valve Gate Was Broke
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Prepared Date
2018-11-07 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Manager Compliance
Authorizer Email
N*******@e****.com
Narrative
On 10/7/2018 at 7:50 am lid 914f-100 (line 9) was lined up to deliver into tank 162. Shortly after start up, operator noticed product leaking on a 10" blind flange on tank 162. The movement was shut down immediately. It was discover that a 10" valve had a broken pin that connected the valve stem to the sealing mechanism inside the valve body. As a result, the valve indicator showed to be open but it remained 100% closed. Additionally, the pressure transmitter that monitored the line pressure had blockage in the port so it did not trigger the sdv to close, resulting in an overpressure. The overpressure caused a leak at the blind flange. No product was recovered. The 10" valve was replaced and the pressure transmitter ports were cleared of debris. Trrc was notified of the accident immediately following confirmation of volume loss exceeding the 5 gallon threshold on 10/8/2018 at 17:26hrs; trrc incident #1857
Report Received Date 2018-11-02 00:00:00
Iyear 2018
Report Number 20180337
Supplemental Number 31146
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-10-07 07:55:00
Location Latitude 29.681722 Google Maps OpenStreetMap
Location Longitude -95.014809 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 1.5
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-10-07 07:55:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-07 07:55:00
Restart Datetime 2018-10-22 08:00:00
On Site Datetime 2018-10-07 07:55:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lid 914f-100
Segment Name Mont Belvieu To Morgans Point #9
Onshore State Abbreviation Tx
Onshore Postal Code 77571
Onshore City Name Morgan's Point
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Mp 0.0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 15000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 15100
Accident Psig 790
Mop Psig 285
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Valve line up was done manual by operations - not by control room
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Additional Other Ind Yes
Eq Additional Other Details Pin That Connects Valve Stem To Valve Gate Was Broke
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Prepared Date 2018-11-07 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Manager Compliance
Authorizer Email N*******@e****.com
Narrative On 10/7/2018 at 7:50 am lid 914f-100 (line 9) was lined up to deliver into tank 162. Shortly after start up, operator noticed product leaking on a 10" blind flange on tank 162. The movement was shut down immediately. It was discover that a 10" valve had a broken pin that connected the valve stem to the sealing mechanism inside the valve body. As a result, the valve indicator showed to be open but it remained 100% closed. Additionally, the pressure transmitter that monitored the line pressure had blockage in the port so it did not trigger the sdv to close, resulting in an overpressure. The overpressure caused a leak at the blind flange. No product was recovered. The 10" valve was replaced and the pressure transmitter ports were cleared of debris. Trrc was notified of the accident immediately following confirmation of volume loss exceeding the 5 gallon threshold on 10/8/2018 at 17:26hrs; trrc incident #1857

All rights reserved. Copyright © by ClearPHMSA