HL incident on 2018-10-14 — TX

Operator
Enable Midstream Partners, Lp
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$48,200
Incident datetime
2018-10-14 15:49
Report number
Location
TX
Narrative
On 10-14-18 a leak was found by a land owner in harrison county, texas. The landowner immediately notified enable gas transmission system control. An o&m technician was dispatched to verify if the leak and it was confirmed that line aj-3 was leaking. The responding employees then contacted gas control and the harrison co sheriff's office. The line was taken out of service and a repair was made. During the release, the liquid ethane immediately vaporized when exposed to air resulting in a large ice crater at the leak site. Field examination of the line showed localized pitting with a pinhole in the pipeline. The defect was removed and sent for analysis. The results of the analysis have not been completed and a supplemental report will be submitted when the analysis is received. The incident was reported to the nrc on 10/14/2018 at 19:29 cst (nrc #1227477) and the 48 hour follow up (1227588) was provided on 10/16/2018 09:15. Enable received the metallurgical report from the lab. The lab confirmed the cause of the pinhole was stray current corrosion, but could not identify specifically ac or dc. Enable field investigations and measurements lead US to believe that it was stray ac current. Supplemental 3/20/2019 part h narrative
Detailed record list
Report Received Date
2018-11-01 00:00:00
Iyear
2018
Report Number
20180334
Supplemental Number
31820
Report Type
Supplemental Final
Operator Id
Name
Enable Midstream Partners, Lp
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-10-14 14:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
1
Intentional Release Bbls
832
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2018-10-14 15:49:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-14 17:00:00
Restart Datetime
2018-10-15 19:30:00
On Site Datetime
2018-10-14 15:49:00
Nrc Rpt Datetime
2018-10-14 19:36:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Line Aj-3
Segment Name
Line Aj-3
Onshore State Abbreviation
Tx
Onshore Postal Code
75602
Onshore City Name
Not Within A Municipality
Onshore County Name
Harrison
Designated Location
Survey Station No.
Designated Name
470+30
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
Api-5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Tex-Tube
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
1997
Manufactured Year
1997
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
6000
Est Cost Gas Released
12230
Est Cost Prop Damage
48200
Est Cost Emergency
5000
Est Cost Environmental
0
Est Cost Other
0
Prpty
71430
Accident Psig
1055
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
26192
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2018
Close Interval Survey Year
2018
Other Cp Survey Year
2018
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2014
Hydrtst Most Rcnt Pressure
2110
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C**** R******
Preparer Title
Lead Dot Compliance Program Manager
Preparer Email
C************@e**************.com
Preparer Telephone
405 558 4647
Prepared Date
2019-03-20 00:00:00
Authorizer Name
C**** R******
Authorizer Telephone
405 558 4647
Authorizer Title
Lead Dot Compliance Program Manager
Authorizer Email
C************@e**************.com
Narrative
On 10-14-18 a leak was found by a land owner in harrison county, texas. The landowner immediately notified enable gas transmission system control. An o&m technician was dispatched to verify if the leak and it was confirmed that line aj-3 was leaking. The responding employees then contacted gas control and the harrison co sheriff's office. The line was taken out of service and a repair was made. During the release, the liquid ethane immediately vaporized when exposed to air resulting in a large ice crater at the leak site. Field examination of the line showed localized pitting with a pinhole in the pipeline. The defect was removed and sent for analysis. The results of the analysis have not been completed and a supplemental report will be submitted when the analysis is received. The incident was reported to the nrc on 10/14/2018 at 19:29 cst (nrc #1227477) and the 48 hour follow up (1227588) was provided on 10/16/2018 09:15. Enable received the metallurgical report from the lab. The lab confirmed the cause of the pinhole was stray current corrosion, but could not identify specifically ac or dc. Enable field investigations and measurements lead US to believe that it was stray ac current. Supplemental 3/20/2019 part h narrative
Report Received Date 2018-11-01 00:00:00
Iyear 2018
Report Number 20180334
Supplemental Number 31820
Report Type Supplemental Final
Operator Id 31202 PHMSA Enforcement
Name Enable Midstream Partners, Lp
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-10-14 14:30:00
Location Latitude 32.42684 Google Maps OpenStreetMap
Location Longitude -94.561733 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 1
Intentional Release Bbls 832
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2018-10-14 15:49:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-14 17:00:00
Restart Datetime 2018-10-15 19:30:00
On Site Datetime 2018-10-14 15:49:00
Nrc Rpt Datetime 2018-10-14 19:36:00
Nrc Rpt Num 1227477 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Line Aj-3
Segment Name Line Aj-3
Onshore State Abbreviation Tx
Onshore Postal Code 75602
Onshore City Name Not Within A Municipality
Onshore County Name Harrison
Designated Location Survey Station No.
Designated Name 470+30
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification Api-5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Tex-Tube
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 1997
Manufactured Year 1997
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 6000
Est Cost Gas Released 12230
Est Cost Prop Damage 48200
Est Cost Emergency 5000
Est Cost Environmental 0
Est Cost Other 0
Prpty 71430
Accident Psig 1055
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 26192
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2018
Close Interval Survey Year 2018
Other Cp Survey Year 2018
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2014
Hydrtst Most Rcnt Pressure 2110
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C**** R******
Preparer Title Lead Dot Compliance Program Manager
Preparer Email C************@e**************.com
Preparer Telephone 405 558 4647
Prepared Date 2019-03-20 00:00:00
Authorizer Name C**** R******
Authorizer Telephone 405 558 4647
Authorizer Title Lead Dot Compliance Program Manager
Authorizer Email C************@e**************.com
Narrative On 10-14-18 a leak was found by a land owner in harrison county, texas. The landowner immediately notified enable gas transmission system control. An o&m technician was dispatched to verify if the leak and it was confirmed that line aj-3 was leaking. The responding employees then contacted gas control and the harrison co sheriff's office. The line was taken out of service and a repair was made. During the release, the liquid ethane immediately vaporized when exposed to air resulting in a large ice crater at the leak site. Field examination of the line showed localized pitting with a pinhole in the pipeline. The defect was removed and sent for analysis. The results of the analysis have not been completed and a supplemental report will be submitted when the analysis is received. The incident was reported to the nrc on 10/14/2018 at 19:29 cst (nrc #1227477) and the 48 hour follow up (1227588) was provided on 10/16/2018 09:15. Enable received the metallurgical report from the lab. The lab confirmed the cause of the pinhole was stray current corrosion, but could not identify specifically ac or dc. Enable field investigations and measurements lead US to believe that it was stray ac current. Supplemental 3/20/2019 part h narrative

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