HL incident on 2018-09-27 — TX

Operator
Kinder Morgan Co2 Co. Lp
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2018-09-27 20:20
Report number
Location
TX
Narrative
On 9/27/2018, a kinder morgan employee identified that a relief valve was activated on eastern shelf pipeline (espl) at the station, tract 142. The employee reported the relief valve to the control center, and then local field operations personnel went to the site to investigate. It was determined that a thermal relief valve was activated. The thermal relief valve was isolated and replaced. Based on a review of pressure data, the pipeline pressures did not exceed normal operating parameters. A visual inspection of the relief valve found that the seat assembly clearance was out of tolerance. The kinder morgan employee who identified the release does not have operational responsibility of the asset, and has not been trained and qualified on emergency response.
Detailed record list
Report Received Date
2018-10-25 00:00:00
Iyear
2018
Report Number
20180327
Supplemental Number
31426
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Co2 Co. Lp
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-09-27 20:20:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
27
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-09-27 20:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Thermal Relief Valve Was Isolated And Replaced.
On Site Datetime
2018-09-27 20:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Eastern Shelf Pipeline
Segment Name
Espl Mp 0
Onshore State Abbreviation
Tx
Onshore Postal Code
79549
Onshore City Name
Snyder
Onshore County Name
Scurry
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2010
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
73
Est Cost Prop Damage
500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
573
Accident Psig
2170
Mop Psig
2220
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pressures at the time of the release were below the maximum control pressure (mcp) and maximum operating pressure (mop) of the eastern shelf pipeline (espl). The controller had not made any changes to the flow or pressure associated with espl prior to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Additional Defect Ind
Yes
Preparer Name
A**** Z*****
Preparer Title
Manager-Regulatory
Preparer Email
A***********@k***********.com
Preparer Telephone
713-369-9512
Preparer Fax
303-984-3417
Prepared Date
2019-01-03 00:00:00
Authorizer Name
M***** L*******
Authorizer Telephone
713-420-4649
Authorizer Title
Director-Operations And Engineering
Authorizer Email
M**************@k***********.com
Narrative
On 9/27/2018, a kinder morgan employee identified that a relief valve was activated on eastern shelf pipeline (espl) at the station, tract 142. The employee reported the relief valve to the control center, and then local field operations personnel went to the site to investigate. It was determined that a thermal relief valve was activated. The thermal relief valve was isolated and replaced. Based on a review of pressure data, the pipeline pressures did not exceed normal operating parameters. A visual inspection of the relief valve found that the seat assembly clearance was out of tolerance. The kinder morgan employee who identified the release does not have operational responsibility of the asset, and has not been trained and qualified on emergency response.
Report Received Date 2018-10-25 00:00:00
Iyear 2018
Report Number 20180327
Supplemental Number 31426
Report Type Supplemental Final
Operator Id 31555 PHMSA Enforcement
Name Kinder Morgan Co2 Co. Lp
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-09-27 20:20:00
Location Latitude 32.758531 Google Maps OpenStreetMap
Location Longitude -100.96057 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 27
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-09-27 20:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Thermal Relief Valve Was Isolated And Replaced.
On Site Datetime 2018-09-27 20:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Eastern Shelf Pipeline
Segment Name Espl Mp 0
Onshore State Abbreviation Tx
Onshore Postal Code 79549
Onshore City Name Snyder
Onshore County Name Scurry
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2010
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 73
Est Cost Prop Damage 500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 573
Accident Psig 2170
Mop Psig 2220
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pressures at the time of the release were below the maximum control pressure (mcp) and maximum operating pressure (mop) of the eastern shelf pipeline (espl). The controller had not made any changes to the flow or pressure associated with espl prior to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Additional Defect Ind Yes
Preparer Name A**** Z*****
Preparer Title Manager-Regulatory
Preparer Email A***********@k***********.com
Preparer Telephone 713-369-9512
Preparer Fax 303-984-3417
Prepared Date 2019-01-03 00:00:00
Authorizer Name M***** L*******
Authorizer Telephone 713-420-4649
Authorizer Title Director-Operations And Engineering
Authorizer Email M**************@k***********.com
Narrative On 9/27/2018, a kinder morgan employee identified that a relief valve was activated on eastern shelf pipeline (espl) at the station, tract 142. The employee reported the relief valve to the control center, and then local field operations personnel went to the site to investigate. It was determined that a thermal relief valve was activated. The thermal relief valve was isolated and replaced. Based on a review of pressure data, the pipeline pressures did not exceed normal operating parameters. A visual inspection of the relief valve found that the seat assembly clearance was out of tolerance. The kinder morgan employee who identified the release does not have operational responsibility of the asset, and has not been trained and qualified on emergency response.

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