HL incident on 2018-09-26 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$45,000
Incident datetime
2018-09-26 11:29
Report number
Location
OK
Narrative
During the aerial patrol of the oneok creek pipeline on 9/26/2018 the pilot observed what appeared to be ice over the pipeline on the downstream side of slick rd. Local oneok field operator was contacted by the pilot and dispatched to the location. Field operator identified ice, dead vegetation and vapors coming on the right-of-way directly above the pipeline. Pipeline control and operations supervisor were contacted and the pipeline was shut down and the location was isolated. Repair crews excavated the pipeline and discovered a pinhole leak. A plidco mechanical repair clamp was installed and the pipeline returned to service. Oneok's investigation determined the interference causing the leak resulted from a negative cable being installed to the casing, instead of the mainline, by a contractor in september of 2017. The cable was associated with a new ground bed that had been installed in june of 2017 with the rectifier at the location being energized in november of 2017. 12/21/2018 correction - corrected part b, question 10 to show accident occurred on pipeline right of way. N.Jones
Detailed record list
Report Received Date
2018-10-24 00:00:00
Iyear
2018
Report Number
20180324
Supplemental Number
31384
Report Type
Supplemental
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-09-26 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
2.7
Intentional Release Bbls
373
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-09-26 11:29:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-09-26 13:08:00
Restart Datetime
2018-09-29 13:00:00
On Site Datetime
2018-09-26 11:29:00
Nrc Rpt Datetime
2018-09-26 13:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Oneok Creek Pipeline
Segment Name
Creek Plant To Carney Plant 6" (Index 10185)
Onshore State Abbreviation
Ok
Onshore Postal Code
74039
Onshore City Name
Not Within A Municipality
Onshore County Name
Creek
Designated Location
Survey Station No.
Designated Name
2750+69
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Textube
Pipe Coating Type
Cold Applied Tape
Installation Year
1986
Manufactured Year
1986
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
13220
Est Cost Prop Damage
45000
Est Cost Emergency
200
Est Cost Environmental
0
Est Cost Other
0
Prpty
58420
Accident Psig
760
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
22705
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place prior to the release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Interference Caused By Improper Negative Cable Installation
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1986
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2017
Prior Damage
Yes
Collected Data Ind
Yes
Other Recent Year
2015
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Manager
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2018-12-21 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
N*********@o****.com
Narrative
During the aerial patrol of the oneok creek pipeline on 9/26/2018 the pilot observed what appeared to be ice over the pipeline on the downstream side of slick rd. Local oneok field operator was contacted by the pilot and dispatched to the location. Field operator identified ice, dead vegetation and vapors coming on the right-of-way directly above the pipeline. Pipeline control and operations supervisor were contacted and the pipeline was shut down and the location was isolated. Repair crews excavated the pipeline and discovered a pinhole leak. A plidco mechanical repair clamp was installed and the pipeline returned to service. Oneok's investigation determined the interference causing the leak resulted from a negative cable being installed to the casing, instead of the mainline, by a contractor in september of 2017. The cable was associated with a new ground bed that had been installed in june of 2017 with the rectifier at the location being energized in november of 2017. 12/21/2018 correction - corrected part b, question 10 to show accident occurred on pipeline right of way. N.Jones
Report Received Date 2018-10-24 00:00:00
Iyear 2018
Report Number 20180324
Supplemental Number 31384
Report Type Supplemental
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2018-09-26 11:30:00
Location Latitude 35.9000658 Google Maps OpenStreetMap
Location Longitude -96.227408 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 2.7
Intentional Release Bbls 373
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-09-26 11:29:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-09-26 13:08:00
Restart Datetime 2018-09-29 13:00:00
On Site Datetime 2018-09-26 11:29:00
Nrc Rpt Datetime 2018-09-26 13:15:00
Nrc Rpt Num 1225773 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Oneok Creek Pipeline
Segment Name Creek Plant To Carney Plant 6" (Index 10185)
Onshore State Abbreviation Ok
Onshore Postal Code 74039
Onshore City Name Not Within A Municipality
Onshore County Name Creek
Designated Location Survey Station No.
Designated Name 2750+69
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Textube
Pipe Coating Type Cold Applied Tape
Installation Year 1986
Manufactured Year 1986
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 13220
Est Cost Prop Damage 45000
Est Cost Emergency 200
Est Cost Environmental 0
Est Cost Other 0
Prpty 58420
Accident Psig 760
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 22705
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place prior to the release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Interference Caused By Improper Negative Cable Installation
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1986
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2017
Prior Damage Yes
Collected Data Ind Yes
Other Recent Year 2015
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N*** J****
Preparer Title Requlatory Compliance Manager
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2018-12-21 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Manager
Authorizer Email N*********@o****.com
Narrative During the aerial patrol of the oneok creek pipeline on 9/26/2018 the pilot observed what appeared to be ice over the pipeline on the downstream side of slick rd. Local oneok field operator was contacted by the pilot and dispatched to the location. Field operator identified ice, dead vegetation and vapors coming on the right-of-way directly above the pipeline. Pipeline control and operations supervisor were contacted and the pipeline was shut down and the location was isolated. Repair crews excavated the pipeline and discovered a pinhole leak. A plidco mechanical repair clamp was installed and the pipeline returned to service. Oneok's investigation determined the interference causing the leak resulted from a negative cable being installed to the casing, instead of the mainline, by a contractor in september of 2017. The cable was associated with a new ground bed that had been installed in june of 2017 with the rectifier at the location being energized in november of 2017. 12/21/2018 correction - corrected part b, question 10 to show accident occurred on pipeline right of way. N.Jones

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