HL incident on 2018-10-22 — CO

Operator
Markwest Michigan Pipeline, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-10-22 09:30
Report number
Location
CO
Narrative
Markwest operation's personnel had loaded a pig into the launcher barrel to be pushed with nitrogen to displace the crude oil in the pipeline for abandonment. A 2" drain valve on the launcher barrel was accidentally left partially open allowing crude oil to fill the sump. Eight (8) barrels of crude oil spilled out onto the ground, but was contained on our launcher property. A vacuum truck was on-site for the operation and it was used to sucked up the spilled crude oil that was returned the pipeline system. The contaminated soil was sucked up separately and placed in a contained vessel for testing and non-hazardous disposal.
Detailed record list
Report Received Date
2018-10-23 00:00:00
Iyear
2018
Report Number
20180323
Supplemental Number
31119
Report Type
Supplemental Final
Operator Id
Name
Markwest Michigan Pipeline, Llc
Operator Street Address
1515 Arapahoe St Tower 1, Suite 1600
Operator City Name
Denver
Operator State Abbreviation
CO
Operator Postal Code
80202
Local Datetime
2018-10-22 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
8
Recovered Bbls
8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-10-22 09:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Crude Oil Was Being Displaced From The Pipeline W/nitrogen For Abandonment
On Site Datetime
2018-10-22 09:30:00
Nrc Rpt Datetime
2018-10-23 11:43:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Markwest Michigan Pipeline Company, Llc
Segment Name
North Michigan 10"
Onshore State Abbreviation
Mi
Onshore Postal Code
49646
Onshore City Name
Kalkaska
Onshore County Name
Kalkaska
Designated Location
Milepost/valve Station
Designated Name
At Launcher
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Installation Year
1973
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
1400
Est Cost Environmental
1000
Est Cost Other
0
Prpty
2400
Accident Psig
200
Mop Psig
400
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
5
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Decommissioning
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D***** T******
Preparer Title
Director Of Pipeline Integrity
Preparer Email
D*************@m*******.com
Preparer Telephone
(303) 531-9089
Prepared Date
2018-10-29 00:00:00
Authorizer Name
D***** T******
Authorizer Telephone
303 531-9089
Authorizer Title
Director Of Pipeline Integrity
Authorizer Email
D*************@m*******.com
Narrative
Markwest operation's personnel had loaded a pig into the launcher barrel to be pushed with nitrogen to displace the crude oil in the pipeline for abandonment. A 2" drain valve on the launcher barrel was accidentally left partially open allowing crude oil to fill the sump. Eight (8) barrels of crude oil spilled out onto the ground, but was contained on our launcher property. A vacuum truck was on-site for the operation and it was used to sucked up the spilled crude oil that was returned the pipeline system. The contaminated soil was sucked up separately and placed in a contained vessel for testing and non-hazardous disposal.
Report Received Date 2018-10-23 00:00:00
Iyear 2018
Report Number 20180323
Supplemental Number 31119
Report Type Supplemental Final
Operator Id 31871 PHMSA Enforcement
Name Markwest Michigan Pipeline, Llc
Operator Street Address 1515 Arapahoe St Tower 1, Suite 1600
Operator City Name Denver
Operator State Abbreviation CO
Operator Postal Code 80202
Local Datetime 2018-10-22 09:30:00
Location Latitude 44.7152917 Google Maps OpenStreetMap
Location Longitude -85.2749673 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 8
Recovered Bbls 8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-10-22 09:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Crude Oil Was Being Displaced From The Pipeline W/nitrogen For Abandonment
On Site Datetime 2018-10-22 09:30:00
Nrc Rpt Datetime 2018-10-23 11:43:00
Nrc Rpt Num 1228275 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Markwest Michigan Pipeline Company, Llc
Segment Name North Michigan 10"
Onshore State Abbreviation Mi
Onshore Postal Code 49646
Onshore City Name Kalkaska
Onshore County Name Kalkaska
Designated Location Milepost/valve Station
Designated Name At Launcher
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Scraper/pig Trap
Installation Year 1973
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 1400
Est Cost Environmental 1000
Est Cost Other 0
Prpty 2400
Accident Psig 200
Mop Psig 400
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 5
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Decommissioning
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D***** T******
Preparer Title Director Of Pipeline Integrity
Preparer Email D*************@m*******.com
Preparer Telephone (303) 531-9089
Prepared Date 2018-10-29 00:00:00
Authorizer Name D***** T******
Authorizer Telephone 303 531-9089
Authorizer Title Director Of Pipeline Integrity
Authorizer Email D*************@m*******.com
Narrative Markwest operation's personnel had loaded a pig into the launcher barrel to be pushed with nitrogen to displace the crude oil in the pipeline for abandonment. A 2" drain valve on the launcher barrel was accidentally left partially open allowing crude oil to fill the sump. Eight (8) barrels of crude oil spilled out onto the ground, but was contained on our launcher property. A vacuum truck was on-site for the operation and it was used to sucked up the spilled crude oil that was returned the pipeline system. The contaminated soil was sucked up separately and placed in a contained vessel for testing and non-hazardous disposal.

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