HL incident on 2018-09-20 — TX

Operator
Stateline Crude, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$17,500
Incident datetime
2018-09-20 20:00
Report number
Location
TX
Narrative
Following a localized power outage resulting in the loss of scada communications and the subsequent closure of downstream outlets (terminal tankage and downstream pipelines), the manual operation of a flowback pump allowed the system to overpressure resulting in the failure of a insulating kit on a pipeline flange. The closure of downstream outlets, automated shutdown of all system pumps and handover of control to local operations is normal operating procedure for all control room personnel during power outages resulting in loss of scada communications. In this situation, a contractor working for wpx energy upstream of stateline crude, llc overrode the automatic shutdown of a pump during flowback operations which resulted in the over-pressurization when downstream outlets were closed. This contractor was not doing work for stateline crude, llc and was not hired by stateline crude, llc. The failure investigation found that stateline crude, llc had inadequate procedures regarding producers having access to its plc's. Stateline crude, llc has changed the procedures so now only company personnel have access to overpressure shutdowns on pumps.
Detailed record list
Report Received Date
2018-10-18 00:00:00
Iyear
2018
Report Number
20180318
Supplemental Number
31310
Report Type
Supplemental Final
Operator Id
Name
Stateline Crude, Llc
Operator Street Address
16211 La Cantera Parkway Suite 202
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78256
Local Datetime
2018-09-20 20:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-09-20 20:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-09-20 20:00:00
Restart Datetime
2018-09-24 10:00:00
On Site Datetime
2018-09-20 20:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
16" Mainline South
Segment Name
16" Mainline South
Onshore State Abbreviation
Tx
Onshore Postal Code
79754
Onshore City Name
Not Within A Municipality
Onshore County Name
Loving
Designated Location
Milepost/valve Station
Designated Name
Lindsay T/i
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2017
Material Involved
Material Other Than Carbon Steel
Material Details
Cp Insulation Kit - Tefcon
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
17500
Est Cost Emergency
12500
Est Cost Environmental
6500
Est Cost Other
0
Prpty
36540
Accident Psig
1079
Mop Psig
740
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Length Segment Isolated
4
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Location Resides Between Upstream Receiver And Downstream Launcher.
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Location Between Receiver And Launcher
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Localized Power Failure Impacted Scada Communications. Normal Aoc Procedures Were Implemented.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
A Flowback Crew Working For Wpx Energy Upstream Of Our Pipeline, Manually Operated Our Pumps After They Had Been Shut In By Our Overpressure Protection. This Crew Does Not Work For Stateline Crude, Llc And Is Not One Of Our Contractors. This Crew Was Not Given Authorization To Override Any Safety Related Pressure Controls Or Shutdowns.
Related Inadequate Proc Ind
Yes
Category Type
Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind
No
Preparer Name
J** H******
Preparer Title
Regulatory Analyst
Preparer Email
J*******@h*******.com
Preparer Telephone
210-298-2229
Prepared Date
2018-12-11 00:00:00
Authorizer Name
J***** R*****
Authorizer Telephone
210-278-1547
Authorizer Title
Vp - Operations
Authorizer Email
J******@h*******.com
Narrative
Following a localized power outage resulting in the loss of scada communications and the subsequent closure of downstream outlets (terminal tankage and downstream pipelines), the manual operation of a flowback pump allowed the system to overpressure resulting in the failure of a insulating kit on a pipeline flange. The closure of downstream outlets, automated shutdown of all system pumps and handover of control to local operations is normal operating procedure for all control room personnel during power outages resulting in loss of scada communications. In this situation, a contractor working for wpx energy upstream of stateline crude, llc overrode the automatic shutdown of a pump during flowback operations which resulted in the over-pressurization when downstream outlets were closed. This contractor was not doing work for stateline crude, llc and was not hired by stateline crude, llc. The failure investigation found that stateline crude, llc had inadequate procedures regarding producers having access to its plc's. Stateline crude, llc has changed the procedures so now only company personnel have access to overpressure shutdowns on pumps.
Report Received Date 2018-10-18 00:00:00
Iyear 2018
Report Number 20180318
Supplemental Number 31310
Report Type Supplemental Final
Operator Id 39589 PHMSA Enforcement
Name Stateline Crude, Llc
Operator Street Address 16211 La Cantera Parkway Suite 202
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78256
Local Datetime 2018-09-20 20:00:00
Location Latitude 31.967929 Google Maps OpenStreetMap
Location Longitude -103.865818 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-09-20 20:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-09-20 20:00:00
Restart Datetime 2018-09-24 10:00:00
On Site Datetime 2018-09-20 20:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 16" Mainline South
Segment Name 16" Mainline South
Onshore State Abbreviation Tx
Onshore Postal Code 79754
Onshore City Name Not Within A Municipality
Onshore County Name Loving
Designated Location Milepost/valve Station
Designated Name Lindsay T/i
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2017
Material Involved Material Other Than Carbon Steel
Material Details Cp Insulation Kit - Tefcon
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 17500
Est Cost Emergency 12500
Est Cost Environmental 6500
Est Cost Other 0
Prpty 36540
Accident Psig 1079
Mop Psig 740
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Length Segment Isolated 4
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Location Resides Between Upstream Receiver And Downstream Launcher.
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Location Between Receiver And Launcher
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Localized Power Failure Impacted Scada Communications. Normal Aoc Procedures Were Implemented.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details A Flowback Crew Working For Wpx Energy Upstream Of Our Pipeline, Manually Operated Our Pumps After They Had Been Shut In By Our Overpressure Protection. This Crew Does Not Work For Stateline Crude, Llc And Is Not One Of Our Contractors. This Crew Was Not Given Authorization To Override Any Safety Related Pressure Controls Or Shutdowns.
Related Inadequate Proc Ind Yes
Category Type Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind No
Preparer Name J** H******
Preparer Title Regulatory Analyst
Preparer Email J*******@h*******.com
Preparer Telephone 210-298-2229
Prepared Date 2018-12-11 00:00:00
Authorizer Name J***** R*****
Authorizer Telephone 210-278-1547
Authorizer Title Vp - Operations
Authorizer Email J******@h*******.com
Narrative Following a localized power outage resulting in the loss of scada communications and the subsequent closure of downstream outlets (terminal tankage and downstream pipelines), the manual operation of a flowback pump allowed the system to overpressure resulting in the failure of a insulating kit on a pipeline flange. The closure of downstream outlets, automated shutdown of all system pumps and handover of control to local operations is normal operating procedure for all control room personnel during power outages resulting in loss of scada communications. In this situation, a contractor working for wpx energy upstream of stateline crude, llc overrode the automatic shutdown of a pump during flowback operations which resulted in the over-pressurization when downstream outlets were closed. This contractor was not doing work for stateline crude, llc and was not hired by stateline crude, llc. The failure investigation found that stateline crude, llc had inadequate procedures regarding producers having access to its plc's. Stateline crude, llc has changed the procedures so now only company personnel have access to overpressure shutdowns on pumps.

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