HL incident on 2018-09-17 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-09-17 15:45
Report number
Location
TX
Narrative
On 9/17/2018 at 1545, operations personnel discovered a leak on an 8" temporary piping connection. Operations personnel had just launched a caliper tool on lid 22862 at the mont belvieu east storage facility. The launcher was immediately isolated. It was discovered that an o-ring had failed on the chiksan connection on the temporary piping. The temporary piping was removed and the o-ring sent in for analysis. Lab results concluded the o-ring exhibited signs mechanical cutting or gouging. The results of examination suggests the o-ring was rolled and pinched. Trc was called at 16:51hrs - trc incident # 001857
Detailed record list
Report Received Date
2018-10-15 00:00:00
Iyear
2018
Report Number
20180306
Supplemental Number
31681
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-09-17 15:45:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
9
Intentional Release Bbls
2
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-09-17 15:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Launcher Was Isolated From The Pipeline.
On Site Datetime
2018-09-17 15:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
24"east-North Y-Grade Line
Segment Name
Lid22862
Onshore State Abbreviation
Tx
Onshore Postal Code
77580
Onshore City Name
Mont Belvieu
Onshore County Name
Chambers
Designated Location
Milepost/valve Station
Designated Name
4.38
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
O-Ring On Chicksan Connection
Installation Year
2018
Material Involved
Material Other Than Carbon Steel
Material Details
90 Duro Fkm (Viton)
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1000
Accident Psig
1120
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
24
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Temporary piping is not under pipeline controller's control.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Exhibited Signs Mechanical Cutting Or Gouging
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Prepared Date
2019-02-20 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Compliance Manager
Authorizer Email
N*******@e****.com
Narrative
On 9/17/2018 at 1545, operations personnel discovered a leak on an 8" temporary piping connection. Operations personnel had just launched a caliper tool on lid 22862 at the mont belvieu east storage facility. The launcher was immediately isolated. It was discovered that an o-ring had failed on the chiksan connection on the temporary piping. The temporary piping was removed and the o-ring sent in for analysis. Lab results concluded the o-ring exhibited signs mechanical cutting or gouging. The results of examination suggests the o-ring was rolled and pinched. Trc was called at 16:51hrs - trc incident # 001857
Report Received Date 2018-10-15 00:00:00
Iyear 2018
Report Number 20180306
Supplemental Number 31681
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-09-17 15:45:00
Location Latitude 29.843971 Google Maps OpenStreetMap
Location Longitude -94.892031 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 9
Intentional Release Bbls 2
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-09-17 15:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Launcher Was Isolated From The Pipeline.
On Site Datetime 2018-09-17 15:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 24"east-North Y-Grade Line
Segment Name Lid22862
Onshore State Abbreviation Tx
Onshore Postal Code 77580
Onshore City Name Mont Belvieu
Onshore County Name Chambers
Designated Location Milepost/valve Station
Designated Name 4.38
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details O-Ring On Chicksan Connection
Installation Year 2018
Material Involved Material Other Than Carbon Steel
Material Details 90 Duro Fkm (Viton)
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1000
Accident Psig 1120
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 24
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Temporary piping is not under pipeline controller's control.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Exhibited Signs Mechanical Cutting Or Gouging
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Prepared Date 2019-02-20 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Compliance Manager
Authorizer Email N*******@e****.com
Narrative On 9/17/2018 at 1545, operations personnel discovered a leak on an 8" temporary piping connection. Operations personnel had just launched a caliper tool on lid 22862 at the mont belvieu east storage facility. The launcher was immediately isolated. It was discovered that an o-ring had failed on the chiksan connection on the temporary piping. The temporary piping was removed and the o-ring sent in for analysis. Lab results concluded the o-ring exhibited signs mechanical cutting or gouging. The results of examination suggests the o-ring was rolled and pinched. Trc was called at 16:51hrs - trc incident # 001857

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