HL incident on 2018-09-15 — TX

Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2018-09-15 11:40
Report number
Location
TX
Narrative
Approximately 2 bbls of crude oil were released as a result of a seal failure on the lynch station delivery booster pump, which caused the catch pan to overfill. The failure was a result of normal wear on the seal. The seal was replaced and this pump has been put back into service.
Detailed record list
Report Received Date
2018-10-10 00:00:00
Iyear
2018
Report Number
20180299
Supplemental Number
31048
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-09-15 11:39:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2018-09-15 11:40:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-09-15 11:39:00
Restart Datetime
2018-09-16 10:17:00
On Site Datetime
2018-09-15 12:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lynch Station
Segment Name
Delivery Booster #2
Onshore State Abbreviation
Nm
Onshore Postal Code
88231
Onshore City Name
Eunice
Onshore County Name
Lea
Designated Location
Milepost/valve Station
Designated Name
Booster #2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
1993
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
140
Est Cost Prop Damage
2500
Est Cost Emergency
3500
Est Cost Environmental
10000
Est Cost Other
0
Prpty
16140
Accident Psig
25
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear Over Time
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
7139935080
Prepared Date
2018-10-10 00:00:00
Authorizer Name
N***** G*****
Authorizer Telephone
713-646-4336
Authorizer Title
Sr Dir Environmental And Regulatory Compliance
Authorizer Email
N******@p****.com
Narrative
Approximately 2 bbls of crude oil were released as a result of a seal failure on the lynch station delivery booster pump, which caused the catch pan to overfill. The failure was a result of normal wear on the seal. The seal was replaced and this pump has been put back into service.
Report Received Date 2018-10-10 00:00:00
Iyear 2018
Report Number 20180299
Supplemental Number 31048
Report Type Original Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-09-15 11:39:00
Location Latitude 32.532861 Google Maps OpenStreetMap
Location Longitude -103.545529 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2018-09-15 11:40:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-09-15 11:39:00
Restart Datetime 2018-09-16 10:17:00
On Site Datetime 2018-09-15 12:25:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lynch Station
Segment Name Delivery Booster #2
Onshore State Abbreviation Nm
Onshore Postal Code 88231
Onshore City Name Eunice
Onshore County Name Lea
Designated Location Milepost/valve Station
Designated Name Booster #2
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 1993
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 140
Est Cost Prop Damage 2500
Est Cost Emergency 3500
Est Cost Environmental 10000
Est Cost Other 0
Prpty 16140
Accident Psig 25
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear Over Time
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 7139935080
Prepared Date 2018-10-10 00:00:00
Authorizer Name N***** G*****
Authorizer Telephone 713-646-4336
Authorizer Title Sr Dir Environmental And Regulatory Compliance
Authorizer Email N******@p****.com
Narrative Approximately 2 bbls of crude oil were released as a result of a seal failure on the lynch station delivery booster pump, which caused the catch pan to overfill. The failure was a result of normal wear on the seal. The seal was replaced and this pump has been put back into service.

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