Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2018-09-15 — TX
Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,500
Incident datetime
2018-09-15 11:40
Report number
Location
TX
Narrative
Approximately 2 bbls of crude oil were released as a result of a seal failure on the lynch station delivery booster pump, which caused the catch pan to overfill. The failure was a result of normal wear on the seal. The seal was replaced and this pump has been put back into service.
Detailed record list
Report Received Date
2018-10-10 00:00:00
Iyear
2018
Report Number
20180299
Supplemental Number
31048
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-09-15 11:39:00
Location Latitude
32.532861
Location Longitude
-103.545529
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2018-09-15 11:40:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-09-15 11:39:00
Restart Datetime
2018-09-16 10:17:00
On Site Datetime
2018-09-15 12:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lynch Station
Segment Name
Delivery Booster #2
Onshore State Abbreviation
Nm
Onshore Postal Code
88231
Onshore City Name
Eunice
Onshore County Name
Lea
Designated Location
Milepost/valve Station
Designated Name
Booster #2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
1993
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
140
Est Cost Prop Damage
2500
Est Cost Emergency
3500
Est Cost Environmental
10000
Est Cost Other
0
Prpty
16140
Accident Psig
25
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear Over Time
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
7139935080
Prepared Date
2018-10-10 00:00:00
Authorizer Name
N***** G*****
Authorizer Telephone
713-646-4336
Authorizer Title
Sr Dir Environmental And Regulatory Compliance
Authorizer Email
N******@p****.com
Narrative
Approximately 2 bbls of crude oil were released as a result of a seal failure on the lynch station delivery booster pump, which caused the catch pan to overfill. The failure was a result of normal wear on the seal. The seal was replaced and this pump has been put back into service.
| Report Received Date | 2018-10-10 00:00:00 |
|---|---|
| Iyear | 2018 |
| Report Number | 20180299 |
| Supplemental Number | 31048 |
| Report Type | Original Final |
| Operator Id | 300 PHMSA Enforcement |
| Name | Plains Pipeline, L.p. |
| Operator Street Address | 333 Clay Street, Suite 1900 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2018-09-15 11:39:00 |
| Location Latitude | 32.532861 Google Maps OpenStreetMap |
| Location Longitude | -103.545529 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Recovered Bbls | 2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Controller |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2018-09-15 11:40:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2018-09-15 11:39:00 |
| Restart Datetime | 2018-09-16 10:17:00 |
| On Site Datetime | 2018-09-15 12:25:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Lynch Station |
| Segment Name | Delivery Booster #2 |
| Onshore State Abbreviation | Nm |
| Onshore Postal Code | 88231 |
| Onshore City Name | Eunice |
| Onshore County Name | Lea |
| Designated Location | Milepost/valve Station |
| Designated Name | Booster #2 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Pump |
| Installation Year | 1993 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 140 |
| Est Cost Prop Damage | 2500 |
| Est Cost Emergency | 3500 |
| Est Cost Environmental | 10000 |
| Est Cost Other | 0 |
| Prpty | 16140 |
| Accident Psig | 25 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest Schedule Ind | Yes |
| Invest No Control Room Ind | Yes |
| Invest No Controller Ind | Yes |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Other Pump Ind | Seal/packing Failure |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Normal Wear Over Time |
| Preparer Name | C******* C***** |
| Preparer Title | Compliance Specialist |
| Preparer Email | C*******@p****.com |
| Preparer Telephone | 7139935080 |
| Prepared Date | 2018-10-10 00:00:00 |
| Authorizer Name | N***** G***** |
| Authorizer Telephone | 713-646-4336 |
| Authorizer Title | Sr Dir Environmental And Regulatory Compliance |
| Authorizer Email | N******@p****.com |
| Narrative | Approximately 2 bbls of crude oil were released as a result of a seal failure on the lynch station delivery booster pump, which caused the catch pan to overfill. The failure was a result of normal wear on the seal. The seal was replaced and this pump has been put back into service. |
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