HL incident on 2018-09-08 — CO

Operator
Western Refining Pipeline, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$138,694
Incident datetime
2018-09-08 13:26
Report number
Location
CO
Narrative
On saturday, september 8 at approximately 1:26 pm (mdt), a release of crude oil from two piping components was discovered at the hospah station in nm. The crude oil was released and contained on site, with minimal offsite impact. Initial estimated volume is 700+ bbl, based on the amount recovered to date. The pipeline was shut down and system isolations were completed. Operations initiated emergency response and stood up local incident command. Spill response support was called out. Required nrc and nmocd notifications have been made. Site clean-up is ongoing to remove impacted soils. An investigation has been initiated to identify lessons learned. Volumes released have remained as stated in part a, 9-11. Investigations are ongoing including supporting PHMSA inspector thomas warner onsite and at the san antonio control center. Upon investigation conclusions the final f 7000.1 report will include any additional information when it is made available. Andeavor is in cooperation with the nmocd for soil remediation. The investigation report has been provided to thomas warner, 12/18/18. Supplemental report submitted to report part d, 8 estimated costs. The direct cause of failure for this incident were cracked welds due to vibration. The metallurgical analysis determined the cause was cracked welds caused by vibration.
Detailed record list
Report Received Date
2018-10-08 00:00:00
Iyear
2018
Report Number
20180297
Supplemental Number
31990
Report Type
Supplemental Final
Operator Id
Name
Western Refining Pipeline, Llc
Operator Street Address
1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name
Denver
Operator State Abbreviation
CO
Operator Postal Code
80202
Local Datetime
2018-09-08 13:26:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
925
Recovered Bbls
821
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-09-08 13:26:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-09-08 13:26:00
Still Shutdown Ind
Yes
On Site Datetime
2018-09-08 13:26:00
Nrc Rpt Datetime
2018-09-08 16:03:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hospah Station
Segment Name
East Line 6"
Onshore State Abbreviation
Nm
Onshore Postal Code
87013
Onshore City Name
Not Within A Municipality
Onshore County Name
Mckinley
Designated Location
Milepost/valve Station
Designated Name
El Bv 24
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Other Butt Weld
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7114
Est Cost Prop Damage
138694
Est Cost Emergency
107001
Est Cost Environmental
218175
Est Cost Other
0
Prpty
470984
Accident Psig
519
Mop Psig
1417
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Other Ind
Yes
Invest Other Ind Details
The Investigation Report Has Been Provided To Thomas Warner-Phmsa, 12/18/18.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Field Exam Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Other
Stress Details
Crack Caused By Vibration
Additional Crack Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2014
Hydrtst Most Rcnt Pressure
1900
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Radiography Rcnt Year
2014
Exm Radiography Rcnt Ind
Yes
Preparer Name
D*** R*******
Preparer Title
Hes Professional
Preparer Email
D***************@a*******.com
Preparer Telephone
5056328006
Preparer Fax
5056324021
Prepared Date
2019-04-18 00:00:00
Authorizer Name
A***** R********
Authorizer Telephone
2106264262
Authorizer Title
Manager Dot Compliance
Authorizer Email
A***************@a*******.com
Narrative
On saturday, september 8 at approximately 1:26 pm (mdt), a release of crude oil from two piping components was discovered at the hospah station in nm. The crude oil was released and contained on site, with minimal offsite impact. Initial estimated volume is 700+ bbl, based on the amount recovered to date. The pipeline was shut down and system isolations were completed. Operations initiated emergency response and stood up local incident command. Spill response support was called out. Required nrc and nmocd notifications have been made. Site clean-up is ongoing to remove impacted soils. An investigation has been initiated to identify lessons learned. Volumes released have remained as stated in part a, 9-11. Investigations are ongoing including supporting PHMSA inspector thomas warner onsite and at the san antonio control center. Upon investigation conclusions the final f 7000.1 report will include any additional information when it is made available. Andeavor is in cooperation with the nmocd for soil remediation. The investigation report has been provided to thomas warner, 12/18/18. Supplemental report submitted to report part d, 8 estimated costs. The direct cause of failure for this incident were cracked welds due to vibration. The metallurgical analysis determined the cause was cracked welds caused by vibration.
Report Received Date 2018-10-08 00:00:00
Iyear 2018
Report Number 20180297
Supplemental Number 31990
Report Type Supplemental Final
Operator Id 31574 PHMSA Enforcement
Name Western Refining Pipeline, Llc
Operator Street Address 1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name Denver
Operator State Abbreviation CO
Operator Postal Code 80202
Local Datetime 2018-09-08 13:26:00
Location Latitude 35.73283 Google Maps OpenStreetMap
Location Longitude -107.74805 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 925
Recovered Bbls 821
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-09-08 13:26:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-09-08 13:26:00
Still Shutdown Ind Yes
On Site Datetime 2018-09-08 13:26:00
Nrc Rpt Datetime 2018-09-08 16:03:00
Nrc Rpt Num 1224046 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Hospah Station
Segment Name East Line 6"
Onshore State Abbreviation Nm
Onshore Postal Code 87013
Onshore City Name Not Within A Municipality
Onshore County Name Mckinley
Designated Location Milepost/valve Station
Designated Name El Bv 24
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Other Butt Weld
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7114
Est Cost Prop Damage 138694
Est Cost Emergency 107001
Est Cost Environmental 218175
Est Cost Other 0
Prpty 470984
Accident Psig 519
Mop Psig 1417
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Other Ind Yes
Invest Other Ind Details The Investigation Report Has Been Provided To Thomas Warner-Phmsa, 12/18/18.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Field Exam Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Other
Stress Details Crack Caused By Vibration
Additional Crack Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2014
Hydrtst Most Rcnt Pressure 1900
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Radiography Rcnt Year 2014
Exm Radiography Rcnt Ind Yes
Preparer Name D*** R*******
Preparer Title Hes Professional
Preparer Email D***************@a*******.com
Preparer Telephone 5056328006
Preparer Fax 5056324021
Prepared Date 2019-04-18 00:00:00
Authorizer Name A***** R********
Authorizer Telephone 2106264262
Authorizer Title Manager Dot Compliance
Authorizer Email A***************@a*******.com
Narrative On saturday, september 8 at approximately 1:26 pm (mdt), a release of crude oil from two piping components was discovered at the hospah station in nm. The crude oil was released and contained on site, with minimal offsite impact. Initial estimated volume is 700+ bbl, based on the amount recovered to date. The pipeline was shut down and system isolations were completed. Operations initiated emergency response and stood up local incident command. Spill response support was called out. Required nrc and nmocd notifications have been made. Site clean-up is ongoing to remove impacted soils. An investigation has been initiated to identify lessons learned. Volumes released have remained as stated in part a, 9-11. Investigations are ongoing including supporting PHMSA inspector thomas warner onsite and at the san antonio control center. Upon investigation conclusions the final f 7000.1 report will include any additional information when it is made available. Andeavor is in cooperation with the nmocd for soil remediation. The investigation report has been provided to thomas warner, 12/18/18. Supplemental report submitted to report part d, 8 estimated costs. The direct cause of failure for this incident were cracked welds due to vibration. The metallurgical analysis determined the cause was cracked welds caused by vibration.

All rights reserved. Copyright © by ClearPHMSA