HL incident on 2018-09-08 — TX

Operator
Plains Marketing, L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-09-08 09:30
Report number
Location
TX
Narrative
Approximately 20 bbls of crude oil were released during a maintenance-related activity to mitigate low flow/no flow condition on facility manifold piping. The line segment had been isolated and drained in advance of the final valve removal, but due to a vapor lock situation, oil was released as valve was unbolted and removed. After the flow subsided the valve was bolted back into place. Plains is working to verify and update facility drawings to identify all drains. Supplemental narrative: part g, #5 has been corrected.
Detailed record list
Report Received Date
2018-10-08 00:00:00
Iyear
2018
Report Number
20180294
Supplemental Number
32059
Report Type
Supplemental Final
Operator Id
Name
Plains Marketing, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-09-08 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-09-08 09:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shut Down And Drained Prior To Maintenance Activities.
On Site Datetime
2018-09-08 09:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Saint James Terminal
Segment Name
1200 Manifold
Onshore State Abbreviation
La
Onshore Postal Code
70086
Onshore City Name
Saint James
Onshore County Name
Saint James
Designated Location
Milepost/valve Station
Designated Name
1200 Manifold
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2005
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Release Of Piping Vapor Lock
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
0
Est Cost Emergency
16000
Est Cost Environmental
7500
Est Cost Other
0
Prpty
24500
Accident Psig
0
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This pipeline segment was isolated and taken out of service at the time of the incident. The segment was purged and locked out/tagged out, and was not visible to the controller due to isolation in preparation for maintenance activities.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Num Contractors Tested
5
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Vapor Lock Within The Line Segment Limited Proper Drain Down Of Line Segment Prior To Maintenance Activity (Valve Removal).
Related No Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
7139935080
Prepared Date
2019-05-02 00:00:00
Authorizer Name
N***** G*****
Authorizer Telephone
7136464336
Authorizer Title
Sr Dir Environmental And Regulatory Compliance
Authorizer Email
N******@p****.com
Narrative
Approximately 20 bbls of crude oil were released during a maintenance-related activity to mitigate low flow/no flow condition on facility manifold piping. The line segment had been isolated and drained in advance of the final valve removal, but due to a vapor lock situation, oil was released as valve was unbolted and removed. After the flow subsided the valve was bolted back into place. Plains is working to verify and update facility drawings to identify all drains. Supplemental narrative: part g, #5 has been corrected.
Report Received Date 2018-10-08 00:00:00
Iyear 2018
Report Number 20180294
Supplemental Number 32059
Report Type Supplemental Final
Operator Id 26085 PHMSA Enforcement
Name Plains Marketing, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-09-08 09:30:00
Location Latitude 30.003623 Google Maps OpenStreetMap
Location Longitude -90.855824 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 20
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-09-08 09:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shut Down And Drained Prior To Maintenance Activities.
On Site Datetime 2018-09-08 09:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Saint James Terminal
Segment Name 1200 Manifold
Onshore State Abbreviation La
Onshore Postal Code 70086
Onshore City Name Saint James
Onshore County Name Saint James
Designated Location Milepost/valve Station
Designated Name 1200 Manifold
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2005
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Release Of Piping Vapor Lock
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 0
Est Cost Emergency 16000
Est Cost Environmental 7500
Est Cost Other 0
Prpty 24500
Accident Psig 0
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This pipeline segment was isolated and taken out of service at the time of the incident. The segment was purged and locked out/tagged out, and was not visible to the controller due to isolation in preparation for maintenance activities.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Num Contractors Tested 5
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Vapor Lock Within The Line Segment Limited Proper Drain Down Of Line Segment Prior To Maintenance Activity (Valve Removal).
Related No Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 7139935080
Prepared Date 2019-05-02 00:00:00
Authorizer Name N***** G*****
Authorizer Telephone 7136464336
Authorizer Title Sr Dir Environmental And Regulatory Compliance
Authorizer Email N******@p****.com
Narrative Approximately 20 bbls of crude oil were released during a maintenance-related activity to mitigate low flow/no flow condition on facility manifold piping. The line segment had been isolated and drained in advance of the final valve removal, but due to a vapor lock situation, oil was released as valve was unbolted and removed. After the flow subsided the valve was bolted back into place. Plains is working to verify and update facility drawings to identify all drains. Supplemental narrative: part g, #5 has been corrected.

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