HL incident on 2018-08-23 — OK

Operator
Velocity Central Oklahoma Pipeline, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2018-08-23 04:27
Report number
Location
OK
Narrative
Release occurred due to a fitting connected to a pump failed/cracked due to vibration. Released crude oil was contained on the facility property and adjacent right of way. Impacted soil was excavated and replaced with clean.
Detailed record list
Report Received Date
2018-10-02 00:00:00
Iyear
2018
Report Number
20180289
Supplemental Number
31016
Report Type
Supplemental Final
Operator Id
Name
Velocity Central Oklahoma Pipeline, Llc
Operator Street Address
Po Box 769
Operator City Name
Lindsay
Operator State Abbreviation
OK
Operator Postal Code
73052
Local Datetime
2018-08-23 04:27:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
8
Recovered Bbls
8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-08-23 04:27:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-08-23 04:27:00
Restart Datetime
2018-08-23 07:23:00
On Site Datetime
2018-08-23 05:29:00
Nrc Rpt Datetime
2018-08-23 09:42:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Alex Terminal
Segment Name
Alex Terminal
Onshore State Abbreviation
Ok
Onshore Postal Code
73002
Onshore City Name
Alex
Onshore County Name
Grady
Designated Location
Milepost/valve Station
Designated Name
Alex Terminal
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
600
Est Cost Prop Damage
1000
Est Cost Emergency
1000
Est Cost Environmental
61000
Est Cost Other
0
Prpty
63600
Accident Psig
585
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak discovered from failure in fitting and manually shutdown within moments of release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Preparer Name
T**** H*****
Preparer Title
Project Manager
Preparer Email
T***********@o**********.net
Preparer Telephone
888-584-3386
Prepared Date
2018-10-05 00:00:00
Authorizer Name
M*** P*****
Authorizer Telephone
918-574-2324
Authorizer Title
Vice President And Cfo
Authorizer Email
M******@v****************.com
Narrative
Release occurred due to a fitting connected to a pump failed/cracked due to vibration. Released crude oil was contained on the facility property and adjacent right of way. Impacted soil was excavated and replaced with clean.
Report Received Date 2018-10-02 00:00:00
Iyear 2018
Report Number 20180289
Supplemental Number 31016
Report Type Supplemental Final
Operator Id 39358 PHMSA Enforcement
Name Velocity Central Oklahoma Pipeline, Llc
Operator Street Address Po Box 769
Operator City Name Lindsay
Operator State Abbreviation OK
Operator Postal Code 73052
Local Datetime 2018-08-23 04:27:00
Location Latitude 34.89906 Google Maps OpenStreetMap
Location Longitude -97.760908 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 8
Recovered Bbls 8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-08-23 04:27:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-08-23 04:27:00
Restart Datetime 2018-08-23 07:23:00
On Site Datetime 2018-08-23 05:29:00
Nrc Rpt Datetime 2018-08-23 09:42:00
Nrc Rpt Num 1222434 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Alex Terminal
Segment Name Alex Terminal
Onshore State Abbreviation Ok
Onshore Postal Code 73002
Onshore City Name Alex
Onshore County Name Grady
Designated Location Milepost/valve Station
Designated Name Alex Terminal
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 600
Est Cost Prop Damage 1000
Est Cost Emergency 1000
Est Cost Environmental 61000
Est Cost Other 0
Prpty 63600
Accident Psig 585
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak discovered from failure in fitting and manually shutdown within moments of release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Preparer Name T**** H*****
Preparer Title Project Manager
Preparer Email T***********@o**********.net
Preparer Telephone 888-584-3386
Prepared Date 2018-10-05 00:00:00
Authorizer Name M*** P*****
Authorizer Telephone 918-574-2324
Authorizer Title Vice President And Cfo
Authorizer Email M******@v****************.com
Narrative Release occurred due to a fitting connected to a pump failed/cracked due to vibration. Released crude oil was contained on the facility property and adjacent right of way. Impacted soil was excavated and replaced with clean.

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