HL incident on 2018-08-28 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$75
Incident datetime
2018-08-28 10:05
Report number
Location
OK
Narrative
At approximately 10:05 on 8/28/2018 oneok pipeline control center received hazardous atmosphere alarms for oneok's arbuckle pipeline middleton pump station. The alarm activated the pump shutdown and station isolation. Oneok pipeline control center controller notified field personnel of the alarm and dispatched a oneok representative to the location. Upon arrival, the oneok representative identified gasket between flanges on the pump header to be the source of the release. He then further isolated the segment and began to purge the section of hydrocarbons. The failed gasket was removed and replaced with a new gasket and new bolts were installed and torqued to manufactures specifications and the station was returned to service.
Detailed record list
Report Received Date
2018-09-27 00:00:00
Iyear
2018
Report Number
20180285
Supplemental Number
30999
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-08-28 10:05:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
19
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-08-28 10:05:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-08-28 10:05:00
Restart Datetime
2018-08-28 18:27:00
On Site Datetime
2018-08-28 11:40:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Middleton Pump Station
Segment Name
Oneok Arbuckle Pipeline Index # 10484
Onshore State Abbreviation
Tx
Onshore Postal Code
75833
Onshore City Name
Not Within A Municipality
Onshore County Name
Leon
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2008
Material Involved
Material Other Than Carbon Steel
Material Details
Flexitallic Gasket
Release Type
Leak
Leak Type
Other
Leak Type Other
Flexitallic Gasket
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
760
Est Cost Prop Damage
75
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
0
Prpty
1335
Accident Psig
415
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
Failure Of Gasket
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Manager
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2018-10-01 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
N*********@o****.com
Narrative
At approximately 10:05 on 8/28/2018 oneok pipeline control center received hazardous atmosphere alarms for oneok's arbuckle pipeline middleton pump station. The alarm activated the pump shutdown and station isolation. Oneok pipeline control center controller notified field personnel of the alarm and dispatched a oneok representative to the location. Upon arrival, the oneok representative identified gasket between flanges on the pump header to be the source of the release. He then further isolated the segment and began to purge the section of hydrocarbons. The failed gasket was removed and replaced with a new gasket and new bolts were installed and torqued to manufactures specifications and the station was returned to service.
Report Received Date 2018-09-27 00:00:00
Iyear 2018
Report Number 20180285
Supplemental Number 30999
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2018-08-28 10:05:00
Location Latitude 31.154358 Google Maps OpenStreetMap
Location Longitude -95.80716 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 19
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-08-28 10:05:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-08-28 10:05:00
Restart Datetime 2018-08-28 18:27:00
On Site Datetime 2018-08-28 11:40:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Middleton Pump Station
Segment Name Oneok Arbuckle Pipeline Index # 10484
Onshore State Abbreviation Tx
Onshore Postal Code 75833
Onshore City Name Not Within A Municipality
Onshore County Name Leon
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2008
Material Involved Material Other Than Carbon Steel
Material Details Flexitallic Gasket
Release Type Leak
Leak Type Other
Leak Type Other Flexitallic Gasket
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 760
Est Cost Prop Damage 75
Est Cost Emergency 500
Est Cost Environmental 0
Est Cost Other 0
Prpty 1335
Accident Psig 415
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Eq Additional Other Ind Yes
Eq Additional Other Details Failure Of Gasket
Preparer Name N*** J****
Preparer Title Requlatory Compliance Manager
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2018-10-01 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Manager
Authorizer Email N*********@o****.com
Narrative At approximately 10:05 on 8/28/2018 oneok pipeline control center received hazardous atmosphere alarms for oneok's arbuckle pipeline middleton pump station. The alarm activated the pump shutdown and station isolation. Oneok pipeline control center controller notified field personnel of the alarm and dispatched a oneok representative to the location. Upon arrival, the oneok representative identified gasket between flanges on the pump header to be the source of the release. He then further isolated the segment and began to purge the section of hydrocarbons. The failed gasket was removed and replaced with a new gasket and new bolts were installed and torqued to manufactures specifications and the station was returned to service.

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