HL incident on 2018-08-01 — TX

Operator
Dcp Midstream
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2018-08-01 09:00
Report number
Location
TX
Narrative
On 8/01/18 an intermittent leak was noticed at the packing on the check valve swing arm at the raptor lateral connection within the river hawk pump station. Since the station would have to be taken down in order to replace the check valve the pressures were monitored to minimize the intermittent leak until the replacement check valve was received. On 8/07/18 the river hawk pump station was taken down and the check valve was replaced. Mitigative action: after a review of operations it was determined that the swing arm on the check valve was unnecessary at this location and a standard check valve was installed.
Detailed record list
Report Received Date
2018-09-05 00:00:00
Iyear
2018
Report Number
20180268
Supplemental Number
30904
Report Type
Original Final
Operator Id
Name
Dcp Midstream
Operator Street Address
2331 Citywest Blvd. Hq-08-S812-02
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2018-08-01 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-08-01 09:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Small Leak On A Control Valve Within The Meter Station
On Site Datetime
2018-08-01 09:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Raptor Cv At Riverhawk Ps
Segment Name
Raptor
Onshore State Abbreviation
Tx
Onshore Postal Code
78017
Onshore City Name
Not Within A Municipality
Onshore County Name
Frio County
Designated Location
Milepost/valve Station
Designated Name
Raptor Ms
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
40000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
40020
Accident Psig
400
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers would not be a contributing factor to the leak at the valve
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Packing At Swing Arm Location
Preparer Name
J***** E*****
Preparer Title
Principle Compliance And Integrity Specialist
Preparer Email
J******@d***********.com
Preparer Telephone
713-375-3679
Prepared Date
2018-09-05 00:00:00
Authorizer Name
J*** P*******
Authorizer Telephone
405-605-3859
Authorizer Title
Manager Pipeline Compliance
Authorizer Email
J*********@d***********.com
Narrative
On 8/01/18 an intermittent leak was noticed at the packing on the check valve swing arm at the raptor lateral connection within the river hawk pump station. Since the station would have to be taken down in order to replace the check valve the pressures were monitored to minimize the intermittent leak until the replacement check valve was received. On 8/07/18 the river hawk pump station was taken down and the check valve was replaced. Mitigative action: after a review of operations it was determined that the swing arm on the check valve was unnecessary at this location and a standard check valve was installed.
Report Received Date 2018-09-05 00:00:00
Iyear 2018
Report Number 20180268
Supplemental Number 30904
Report Type Original Final
Operator Id 31130 PHMSA Enforcement
Name Dcp Midstream
Operator Street Address 2331 Citywest Blvd. Hq-08-S812-02
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2018-08-01 09:00:00
Location Latitude 28.776861 Google Maps OpenStreetMap
Location Longitude -99.249762 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-08-01 09:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Small Leak On A Control Valve Within The Meter Station
On Site Datetime 2018-08-01 09:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Raptor Cv At Riverhawk Ps
Segment Name Raptor
Onshore State Abbreviation Tx
Onshore Postal Code 78017
Onshore City Name Not Within A Municipality
Onshore County Name Frio County
Designated Location Milepost/valve Station
Designated Name Raptor Ms
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 40000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 40020
Accident Psig 400
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers would not be a contributing factor to the leak at the valve
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Packing At Swing Arm Location
Preparer Name J***** E*****
Preparer Title Principle Compliance And Integrity Specialist
Preparer Email J******@d***********.com
Preparer Telephone 713-375-3679
Prepared Date 2018-09-05 00:00:00
Authorizer Name J*** P*******
Authorizer Telephone 405-605-3859
Authorizer Title Manager Pipeline Compliance
Authorizer Email J*********@d***********.com
Narrative On 8/01/18 an intermittent leak was noticed at the packing on the check valve swing arm at the raptor lateral connection within the river hawk pump station. Since the station would have to be taken down in order to replace the check valve the pressures were monitored to minimize the intermittent leak until the replacement check valve was received. On 8/07/18 the river hawk pump station was taken down and the check valve was replaced. Mitigative action: after a review of operations it was determined that the swing arm on the check valve was unnecessary at this location and a standard check valve was installed.

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