HL incident on 2018-08-08 — TX

Operator
Sinclair Transportation Company
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2018-08-08 08:52
Report number
Location
TX
Narrative
At 08:13 on 8/8 the magellan control center notified the sinclair control center to shut down its pump at the chase terminal for an specified reason. At 08:52 the magellan terminal manager contacted the sinclair local area operator and informed him that there had been a release out of the sinclair pump seal. Sinclair's chase pump is a gould model 3196 I-frame pump. In this application a 50 hp motor drives the pump. The pump is located within the magellan terminal. Sinclair takes refined product deliveries at this location and ships them to sinclair's denver product terminal via the 15 mile long chase connection pipeline. Sinclair's and magellan initial response was initiated and, since the release happened within magellan's property, magellan took responsibility for the product recovery and clean-up (at sinclair's expense). The subsequent investigation revealed that the outboard/thrust bearing had failed allowing the impeller shaft to travel forward far enough that the faces of the seal parted allowing the release of gasoline. Due to the wear on the impeller it is apparent that over an unknown period of time the outboard/thrust bearing had begun to fail (chronic condition). Eventually the outboard/thrust bearing cages wore enough that the impeller shaft had sufficient lateral travel to allow the seal to separate. The lab analysis of the bearing oil revealed that the oil had been contaminated with water and the oil had been degraded. This contributing factor may have led to the bearing failure.
Detailed record list
Report Received Date
2018-09-04 00:00:00
Iyear
2018
Report Number
20180264
Supplemental Number
32293
Report Type
Supplemental Final
Operator Id
Name
Sinclair Transportation Company
Operator Street Address
2323 Victory Ave. Suite 1400
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2018-08-08 08:13:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
20
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Terminal Operator
Incident Identified Datetime
2018-08-08 08:52:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-08-08 08:17:00
Restart Datetime
2018-08-10 11:19:00
On Site Datetime
2018-08-08 09:30:00
Nrc Rpt Datetime
2018-08-08 09:47:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Chase Connection Pipeline
Segment Name
12
Onshore State Abbreviation
Co
Onshore Postal Code
82011
Onshore City Name
Aurora
Onshore County Name
Adams
Designated Location
Milepost/valve Station
Designated Name
Chase Termina
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
1998
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Est Cost Oper Paid
20000
Est Cost Gas Released
1680
Est Cost Prop Damage
2000
Est Cost Emergency
10000
Est Cost Environmental
424500
Est Cost Other
0
Est Cost Other Details
None
Prpty
458180
Accident Psig
35
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Other
Other Pump Details
Thrust Bearing In Pump Failed Causing The Impeller Shaft To Move And Open Seal
Eq Additional Other Ind
Yes
Eq Additional Other Details
Degraded Bearing Oil
Preparer Name
J******* B****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
J*****@s**********.com
Preparer Telephone
3073283643
Prepared Date
2019-06-17 00:00:00
Authorizer Name
M*** P*******
Authorizer Telephone
8015242852
Authorizer Title
President Sinclair Transportation Company
Authorizer Email
M********@s**********.com
Narrative
At 08:13 on 8/8 the magellan control center notified the sinclair control center to shut down its pump at the chase terminal for an specified reason. At 08:52 the magellan terminal manager contacted the sinclair local area operator and informed him that there had been a release out of the sinclair pump seal. Sinclair's chase pump is a gould model 3196 I-frame pump. In this application a 50 hp motor drives the pump. The pump is located within the magellan terminal. Sinclair takes refined product deliveries at this location and ships them to sinclair's denver product terminal via the 15 mile long chase connection pipeline. Sinclair's and magellan initial response was initiated and, since the release happened within magellan's property, magellan took responsibility for the product recovery and clean-up (at sinclair's expense). The subsequent investigation revealed that the outboard/thrust bearing had failed allowing the impeller shaft to travel forward far enough that the faces of the seal parted allowing the release of gasoline. Due to the wear on the impeller it is apparent that over an unknown period of time the outboard/thrust bearing had begun to fail (chronic condition). Eventually the outboard/thrust bearing cages wore enough that the impeller shaft had sufficient lateral travel to allow the seal to separate. The lab analysis of the bearing oil revealed that the oil had been contaminated with water and the oil had been degraded. This contributing factor may have led to the bearing failure.
Report Received Date 2018-09-04 00:00:00
Iyear 2018
Report Number 20180264
Supplemental Number 32293
Report Type Supplemental Final
Operator Id 15156 PHMSA Enforcement
Name Sinclair Transportation Company
Operator Street Address 2323 Victory Ave. Suite 1400
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75219
Local Datetime 2018-08-08 08:13:00
Location Latitude 39.758951 Google Maps OpenStreetMap
Location Longitude -104.813266 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 20
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Terminal Operator
Incident Identified Datetime 2018-08-08 08:52:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-08-08 08:17:00
Restart Datetime 2018-08-10 11:19:00
On Site Datetime 2018-08-08 09:30:00
Nrc Rpt Datetime 2018-08-08 09:47:00
Nrc Rpt Num 1220889 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Chase Connection Pipeline
Segment Name 12
Onshore State Abbreviation Co
Onshore Postal Code 82011
Onshore City Name Aurora
Onshore County Name Adams
Designated Location Milepost/valve Station
Designated Name Chase Termina
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 1998
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Est Cost Oper Paid 20000
Est Cost Gas Released 1680
Est Cost Prop Damage 2000
Est Cost Emergency 10000
Est Cost Environmental 424500
Est Cost Other 0
Est Cost Other Details None
Prpty 458180
Accident Psig 35
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Other
Other Pump Details Thrust Bearing In Pump Failed Causing The Impeller Shaft To Move And Open Seal
Eq Additional Other Ind Yes
Eq Additional Other Details Degraded Bearing Oil
Preparer Name J******* B****
Preparer Title Regulatory Compliance Coordinator
Preparer Email J*****@s**********.com
Preparer Telephone 3073283643
Prepared Date 2019-06-17 00:00:00
Authorizer Name M*** P*******
Authorizer Telephone 8015242852
Authorizer Title President Sinclair Transportation Company
Authorizer Email M********@s**********.com
Narrative At 08:13 on 8/8 the magellan control center notified the sinclair control center to shut down its pump at the chase terminal for an specified reason. At 08:52 the magellan terminal manager contacted the sinclair local area operator and informed him that there had been a release out of the sinclair pump seal. Sinclair's chase pump is a gould model 3196 I-frame pump. In this application a 50 hp motor drives the pump. The pump is located within the magellan terminal. Sinclair takes refined product deliveries at this location and ships them to sinclair's denver product terminal via the 15 mile long chase connection pipeline. Sinclair's and magellan initial response was initiated and, since the release happened within magellan's property, magellan took responsibility for the product recovery and clean-up (at sinclair's expense). The subsequent investigation revealed that the outboard/thrust bearing had failed allowing the impeller shaft to travel forward far enough that the faces of the seal parted allowing the release of gasoline. Due to the wear on the impeller it is apparent that over an unknown period of time the outboard/thrust bearing had begun to fail (chronic condition). Eventually the outboard/thrust bearing cages wore enough that the impeller shaft had sufficient lateral travel to allow the seal to separate. The lab analysis of the bearing oil revealed that the oil had been contaminated with water and the oil had been degraded. This contributing factor may have led to the bearing failure.

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