HL incident on 2018-08-04 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,383
Incident datetime
2018-08-04 09:00
Report number
Location
TX
Narrative
On august 4, 2018 at 9:00 am, superior terminal personnel discovered a leak on valve 272 attached to tank 17. Approximately 7.5 gallons of crude oil had been released from the valve, the leak originated from the 1/2" body bleed connection to the valve body. This 8" valve which is attached to the tank is blinded off. A small amount of product was sprayed onto the surrounding soil. Less than a cubic yard of contaminated soil was removed and taken to the soil management site for proper disposal. On august 10, 2018, during a scheduled outage, tank 17 was pumped down to working bottoms to accommodate the investigation and repair of the valve. It was discovered that the release was due to thermal pressure buildup. The valve was secured in the partially open position to prevent further thermal pressure buildup in the future. 09/24/2024 - updated by PHMSA per operator approval.
Detailed record list
Report Received Date
2018-08-30 00:00:00
Iyear
2018
Report Number
20180259
Supplemental Number
30876
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2018-08-04 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.18
Recovered Bbls
0.18
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-08-04 09:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Monitored Until Repairs Could Be Made
On Site Datetime
2018-08-04 09:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Superior Terminal
Segment Name
Tank 17 Valve 272
Onshore State Abbreviation
Wi
Onshore Postal Code
54880
Onshore City Name
Superior
Onshore County Name
Douglas
Designated Location
Milepost/valve Station
Designated Name
1098
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Valve Type
Auxiliary Or Other Valve
Tank Vessel Subtype
Other
Tank Vessel Details
Water Draw Valve
Tank Type
Atmospheric
Installation Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
13
Est Cost Prop Damage
4383
Est Cost Emergency
339
Est Cost Environmental
0
Est Cost Other
0
Prpty
4735
Accident Psig
3
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement. Field identified release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Valve Threads
Additional Thermal Ind
Yes
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2018-08-30 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On august 4, 2018 at 9:00 am, superior terminal personnel discovered a leak on valve 272 attached to tank 17. Approximately 7.5 gallons of crude oil had been released from the valve, the leak originated from the 1/2" body bleed connection to the valve body. This 8" valve which is attached to the tank is blinded off. A small amount of product was sprayed onto the surrounding soil. Less than a cubic yard of contaminated soil was removed and taken to the soil management site for proper disposal. On august 10, 2018, during a scheduled outage, tank 17 was pumped down to working bottoms to accommodate the investigation and repair of the valve. It was discovered that the release was due to thermal pressure buildup. The valve was secured in the partially open position to prevent further thermal pressure buildup in the future. 09/24/2024 - updated by PHMSA per operator approval.
Report Received Date 2018-08-30 00:00:00
Iyear 2018
Report Number 20180259
Supplemental Number 30876
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2018-08-04 09:00:00
Location Latitude 46.686998 Google Maps OpenStreetMap
Location Longitude -92.062559 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.18
Recovered Bbls 0.18
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-08-04 09:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Monitored Until Repairs Could Be Made
On Site Datetime 2018-08-04 09:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Superior Terminal
Segment Name Tank 17 Valve 272
Onshore State Abbreviation Wi
Onshore Postal Code 54880
Onshore City Name Superior
Onshore County Name Douglas
Designated Location Milepost/valve Station
Designated Name 1098
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Valve Type Auxiliary Or Other Valve
Tank Vessel Subtype Other
Tank Vessel Details Water Draw Valve
Tank Type Atmospheric
Installation Year 1952
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 13
Est Cost Prop Damage 4383
Est Cost Emergency 339
Est Cost Environmental 0
Est Cost Other 0
Prpty 4735
Accident Psig 3
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement. Field identified release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Valve Threads
Additional Thermal Ind Yes
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2018-08-30 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On august 4, 2018 at 9:00 am, superior terminal personnel discovered a leak on valve 272 attached to tank 17. Approximately 7.5 gallons of crude oil had been released from the valve, the leak originated from the 1/2" body bleed connection to the valve body. This 8" valve which is attached to the tank is blinded off. A small amount of product was sprayed onto the surrounding soil. Less than a cubic yard of contaminated soil was removed and taken to the soil management site for proper disposal. On august 10, 2018, during a scheduled outage, tank 17 was pumped down to working bottoms to accommodate the investigation and repair of the valve. It was discovered that the release was due to thermal pressure buildup. The valve was secured in the partially open position to prevent further thermal pressure buildup in the future. 09/24/2024 - updated by PHMSA per operator approval.

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