HL incident on 2018-07-24 — CO

Operator
Western Refining Pipeline, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2018-07-24 11:53
Report number
Location
CO
Narrative
One inch nipple on discharge line drain broke the threads and caused a spill at hospah station. Approximately 3.8 bbls were spilled. 3.40 bbls were recovered from the environmental skid, and 16 gallons sprayed onto the ground surface. Pumps were immediately shut down and leaking nipple was isolated. The broken nipple has been sent for metallurgical analysis. The part g8 apparent cause selection will be changed to part g6 once we receive the metallurgical analysis, completed. A failure analysis conducted on the leaking threaded vertical pipe nipple revealed that a crack originated at the root of an unengaged thread. The failure mechanism was metal fatigue likely due to vibrational tensile stresses originating from the nearby mainline pump #1. External tensile stresses were exacerbated by the weight of a ball valve attached to the horizontal pipe nipple attached to the 90-degree elbow.
Detailed record list
Report Received Date
2018-08-24 00:00:00
Iyear
2018
Report Number
20180254
Supplemental Number
31374
Report Type
Supplemental Final
Operator Id
Name
Western Refining Pipeline, Llc
Operator Street Address
1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name
Denver
Operator State Abbreviation
CO
Operator Postal Code
80202
Local Datetime
2018-07-24 11:53:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3.8
Recovered Bbls
3.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-07-24 11:53:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-07-24 11:53:00
Restart Datetime
2018-07-24 14:29:00
On Site Datetime
2018-07-24 11:53:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hospah Station
Segment Name
Hospah To Gallup Refinery
Onshore State Abbreviation
Nm
Onshore Postal Code
87045
Onshore City Name
Not Within A Municipality
Onshore County Name
Mckinley
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
1973
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
26
Est Cost Prop Damage
100
Est Cost Emergency
0
Est Cost Environmental
1059
Est Cost Other
0
Prpty
1185
Accident Psig
929
Mop Psig
1130
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
To small of spray to detect.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Preparer Name
D*** R*******
Preparer Title
Senior Regulatory Compliance Specialist
Preparer Email
D***************@a*******.com
Preparer Telephone
5056328006
Preparer Fax
5056324021
Prepared Date
2018-12-20 00:00:00
Authorizer Name
A***** R********
Authorizer Telephone
2106264262
Authorizer Title
Manager Dot Compliance
Authorizer Email
A***************@a*******.com
Narrative
One inch nipple on discharge line drain broke the threads and caused a spill at hospah station. Approximately 3.8 bbls were spilled. 3.40 bbls were recovered from the environmental skid, and 16 gallons sprayed onto the ground surface. Pumps were immediately shut down and leaking nipple was isolated. The broken nipple has been sent for metallurgical analysis. The part g8 apparent cause selection will be changed to part g6 once we receive the metallurgical analysis, completed. A failure analysis conducted on the leaking threaded vertical pipe nipple revealed that a crack originated at the root of an unengaged thread. The failure mechanism was metal fatigue likely due to vibrational tensile stresses originating from the nearby mainline pump #1. External tensile stresses were exacerbated by the weight of a ball valve attached to the horizontal pipe nipple attached to the 90-degree elbow.
Report Received Date 2018-08-24 00:00:00
Iyear 2018
Report Number 20180254
Supplemental Number 31374
Report Type Supplemental Final
Operator Id 31574 PHMSA Enforcement
Name Western Refining Pipeline, Llc
Operator Street Address 1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name Denver
Operator State Abbreviation CO
Operator Postal Code 80202
Local Datetime 2018-07-24 11:53:00
Location Latitude 35.73283 Google Maps OpenStreetMap
Location Longitude -107.74805 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3.8
Recovered Bbls 3.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-07-24 11:53:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-07-24 11:53:00
Restart Datetime 2018-07-24 14:29:00
On Site Datetime 2018-07-24 11:53:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Hospah Station
Segment Name Hospah To Gallup Refinery
Onshore State Abbreviation Nm
Onshore Postal Code 87045
Onshore City Name Not Within A Municipality
Onshore County Name Mckinley
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year 1973
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 26
Est Cost Prop Damage 100
Est Cost Emergency 0
Est Cost Environmental 1059
Est Cost Other 0
Prpty 1185
Accident Psig 929
Mop Psig 1130
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details To small of spray to detect.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Preparer Name D*** R*******
Preparer Title Senior Regulatory Compliance Specialist
Preparer Email D***************@a*******.com
Preparer Telephone 5056328006
Preparer Fax 5056324021
Prepared Date 2018-12-20 00:00:00
Authorizer Name A***** R********
Authorizer Telephone 2106264262
Authorizer Title Manager Dot Compliance
Authorizer Email A***************@a*******.com
Narrative One inch nipple on discharge line drain broke the threads and caused a spill at hospah station. Approximately 3.8 bbls were spilled. 3.40 bbls were recovered from the environmental skid, and 16 gallons sprayed onto the ground surface. Pumps were immediately shut down and leaking nipple was isolated. The broken nipple has been sent for metallurgical analysis. The part g8 apparent cause selection will be changed to part g6 once we receive the metallurgical analysis, completed. A failure analysis conducted on the leaking threaded vertical pipe nipple revealed that a crack originated at the root of an unengaged thread. The failure mechanism was metal fatigue likely due to vibrational tensile stresses originating from the nearby mainline pump #1. External tensile stresses were exacerbated by the weight of a ball valve attached to the horizontal pipe nipple attached to the 90-degree elbow.

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