HL incident on 2018-07-24 — TX

Operator
Dcp Midstream
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$75,000
Incident datetime
2018-07-24 09:38
Report number
Location
TX
Narrative
On 7/24 a dcp employee noticed a release at a valve assembly while preparing for an upcoming ili tool run. The release was temporarily repaired with a pressure contacting clamp until the permanent repair was scheduled. On 7/26 it was noticed that the temporary repair was leaking, and at this time the crew with equipment was in route to perform the permanent repair. 7/29 the flange and gasket were replaced and the repair was complete. This segment, where this valve assembly is located, has two outlets and deliveries are made concurrently , it is believed that due to the fluctuation of volume and pressure the gasket was exposed to greater expansions and contractions. As a preventative measure on this lateral the operation technicians will conduct additional testing around the flanges during the DOT checks at the valve
Detailed record list
Report Received Date
2018-08-24 00:00:00
Iyear
2018
Report Number
20180253
Supplemental Number
31248
Report Type
Supplemental Final
Operator Id
Name
Dcp Midstream
Operator Street Address
2331 Citywest Blvd. Hq-08-S812-02
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2018-07-24 09:38:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
6.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-07-24 09:38:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
A Temp. Pressure Containing Device Was Installed Until A Perm. Repair Sch.
On Site Datetime
2018-07-24 09:38:00
Nrc Rpt Num
Nrc Notification Required But Not Made
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Barnhart Meter Station
Segment Name
N2 Lateral
Onshore State Abbreviation
Tx
Onshore Postal Code
75835
Onshore City Name
Not Within A Municipality
Onshore County Name
Crockett
Designated Location
Milepost/valve Station
Designated Name
Barnhart Ms
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
1996
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
75000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
75020
Accident Psig
540
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers would not be a contributing factor to the leak on a gasket failure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
Segment Dynamic Controls
Preparer Name
J*** P*******
Preparer Title
Manager Pipeline Compliance
Preparer Email
J*********@d***********.com
Preparer Telephone
405-605-3859
Prepared Date
2018-11-30 00:00:00
Authorizer Name
J*** P*******
Authorizer Telephone
405-605-3859
Authorizer Title
Manager Pipeline Compliance
Authorizer Email
J*********@d***********.com
Narrative
On 7/24 a dcp employee noticed a release at a valve assembly while preparing for an upcoming ili tool run. The release was temporarily repaired with a pressure contacting clamp until the permanent repair was scheduled. On 7/26 it was noticed that the temporary repair was leaking, and at this time the crew with equipment was in route to perform the permanent repair. 7/29 the flange and gasket were replaced and the repair was complete. This segment, where this valve assembly is located, has two outlets and deliveries are made concurrently , it is believed that due to the fluctuation of volume and pressure the gasket was exposed to greater expansions and contractions. As a preventative measure on this lateral the operation technicians will conduct additional testing around the flanges during the DOT checks at the valve
Report Received Date 2018-08-24 00:00:00
Iyear 2018
Report Number 20180253
Supplemental Number 31248
Report Type Supplemental Final
Operator Id 31130 PHMSA Enforcement
Name Dcp Midstream
Operator Street Address 2331 Citywest Blvd. Hq-08-S812-02
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2018-07-24 09:38:00
Location Latitude 30.98902 Google Maps OpenStreetMap
Location Longitude -101.0787 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 6.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-07-24 09:38:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain A Temp. Pressure Containing Device Was Installed Until A Perm. Repair Sch.
On Site Datetime 2018-07-24 09:38:00
Nrc Rpt Num Nrc Notification Required But Not Made NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Barnhart Meter Station
Segment Name N2 Lateral
Onshore State Abbreviation Tx
Onshore Postal Code 75835
Onshore City Name Not Within A Municipality
Onshore County Name Crockett
Designated Location Milepost/valve Station
Designated Name Barnhart Ms
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 1996
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 75000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 75020
Accident Psig 540
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers would not be a contributing factor to the leak on a gasket failure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Eq Additional Other Ind Yes
Eq Additional Other Details Segment Dynamic Controls
Preparer Name J*** P*******
Preparer Title Manager Pipeline Compliance
Preparer Email J*********@d***********.com
Preparer Telephone 405-605-3859
Prepared Date 2018-11-30 00:00:00
Authorizer Name J*** P*******
Authorizer Telephone 405-605-3859
Authorizer Title Manager Pipeline Compliance
Authorizer Email J*********@d***********.com
Narrative On 7/24 a dcp employee noticed a release at a valve assembly while preparing for an upcoming ili tool run. The release was temporarily repaired with a pressure contacting clamp until the permanent repair was scheduled. On 7/26 it was noticed that the temporary repair was leaking, and at this time the crew with equipment was in route to perform the permanent repair. 7/29 the flange and gasket were replaced and the repair was complete. This segment, where this valve assembly is located, has two outlets and deliveries are made concurrently , it is believed that due to the fluctuation of volume and pressure the gasket was exposed to greater expansions and contractions. As a preventative measure on this lateral the operation technicians will conduct additional testing around the flanges during the DOT checks at the valve

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