Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2018-07-26 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2018-07-26 09:45
Report number
Location
TX
Narrative
At 09:25 on 7/26/18 a pipeline technician discovered a leak at the facility . At 9:45 it was determined that the leak came from a 1/2 inch threaded nipple that failed on the discharge side of the pump. The facility was shut down and the nipple replaced. Clean up and remediation was performed and facility was available for service. Accidents/incidents caused by equipment failure are trended and tracked in our operational containment program to prevent reoccurrence. Update: 9/19/2018: additionally to prevent reoccurrence, the tubing, nipple, and transmitter located on the downstream side of the pump was removed completely.
Detailed record list
Report Received Date
2018-08-23 00:00:00
Iyear
2018
Report Number
20180251
Supplemental Number
30956
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-07-26 09:25:00
Location Latitude
31.8796
Location Longitude
-102.1258
Commodity Released Type
Crude Oil
Unintentional Release Bbls
66
Recovered Bbls
28
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-07-26 09:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-07-26 09:45:00
Restart Datetime
2018-07-26 10:45:00
On Site Datetime
2018-07-26 09:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Bryant G Station
Segment Name
Bryant G Loop
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Designated Location
Survey Station No.
Designated Name
Bryant G
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
4600
Est Cost Prop Damage
0
Est Cost Emergency
4500
Est Cost Environmental
12000
Est Cost Other
0
Prpty
21100
Accident Psig
369
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Vibration Ind
Yes
Preparer Name
L**** W*******
Preparer Title
Pipeline Compliance Senior Engineer
Preparer Email
L*********@e****.com
Preparer Telephone
713-381-6748
Prepared Date
2018-09-19 00:00:00
Authorizer Name
L**** W*******
Authorizer Telephone
713-381-6748
Authorizer Title
Pipeline Compliance Senior Engineer
Authorizer Email
L*********@e****.com
Narrative
At 09:25 on 7/26/18 a pipeline technician discovered a leak at the facility . At 9:45 it was determined that the leak came from a 1/2 inch threaded nipple that failed on the discharge side of the pump. The facility was shut down and the nipple replaced. Clean up and remediation was performed and facility was available for service. Accidents/incidents caused by equipment failure are trended and tracked in our operational containment program to prevent reoccurrence. Update: 9/19/2018: additionally to prevent reoccurrence, the tubing, nipple, and transmitter located on the downstream side of the pump was removed completely.
| Report Received Date | 2018-08-23 00:00:00 |
|---|---|
| Iyear | 2018 |
| Report Number | 20180251 |
| Supplemental Number | 30956 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2018-07-26 09:25:00 |
| Location Latitude | 31.8796 Google Maps OpenStreetMap |
| Location Longitude | -102.1258 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 66 |
| Recovered Bbls | 28 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2018-07-26 09:45:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2018-07-26 09:45:00 |
| Restart Datetime | 2018-07-26 10:45:00 |
| On Site Datetime | 2018-07-26 09:25:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Bryant G Station |
| Segment Name | Bryant G Loop |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 79706 |
| Onshore City Name | Midland |
| Onshore County Name | Midland |
| Designated Location | Survey Station No. |
| Designated Name | Bryant G |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Instrumentation |
| Installation Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 4600 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 4500 |
| Est Cost Environmental | 12000 |
| Est Cost Other | 0 |
| Prpty | 21100 |
| Accident Psig | 369 |
| Mop Psig | 720 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Controller nor control room were a contributing factor |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Threaded Connection/coupling Failure |
| Eq Failure Type | Threaded Connection/coupling Failure |
| Other Stripped Ind | Threaded Fitting |
| Additional Vibration Ind | Yes |
| Preparer Name | L**** W******* |
| Preparer Title | Pipeline Compliance Senior Engineer |
| Preparer Email | L*********@e****.com |
| Preparer Telephone | 713-381-6748 |
| Prepared Date | 2018-09-19 00:00:00 |
| Authorizer Name | L**** W******* |
| Authorizer Telephone | 713-381-6748 |
| Authorizer Title | Pipeline Compliance Senior Engineer |
| Authorizer Email | L*********@e****.com |
| Narrative | At 09:25 on 7/26/18 a pipeline technician discovered a leak at the facility . At 9:45 it was determined that the leak came from a 1/2 inch threaded nipple that failed on the discharge side of the pump. The facility was shut down and the nipple replaced. Clean up and remediation was performed and facility was available for service. Accidents/incidents caused by equipment failure are trended and tracked in our operational containment program to prevent reoccurrence. Update: 9/19/2018: additionally to prevent reoccurrence, the tubing, nipple, and transmitter located on the downstream side of the pump was removed completely. |
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