HL incident on 2018-07-26 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$22,636
Incident datetime
2018-07-26 11:30
Report number
Location
TX
Narrative
On july 26, 2018 at 11:30 am cdt, pipeline maintenance crews discovered a release of approximately two barrels of crude on the tank 10 outgoing line at the superior terminal. A pinhole was discovered in the 6:00 position adjacent to the weld joining the 45 degree elbow to the pipe. As a precautionary measure, an nde analysis was completed on the second weld associated with the elbow and along the bottom of the pipe in the vicinity of the leak. No other defects or corrosion were observed. An 18 inch sleeve was welded to the pipe on july 27, 2018 and the line was returned to service. The cause of the release has been attributed to isolated internal corrosion. Approximately 150 tons of contaminated soil was disposed of at an approved site.
Detailed record list
Report Received Date
2018-08-23 00:00:00
Iyear
2018
Report Number
20180250
Supplemental Number
30844
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2018-07-26 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-07-26 11:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Line Was Isolated
On Site Datetime
2018-07-26 11:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Superior Terminal
Segment Name
Tank 10 Piping
Onshore State Abbreviation
Wi
Onshore Postal Code
54880
Onshore City Name
Superior
Onshore County Name
Douglas
Designated Location
Milepost/valve Station
Designated Name
1098
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
34
Pipe Wall Thickness
0.281
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Extruded Polyehylene
Weld Subtype
Pipe Girth Weld
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
140
Est Cost Prop Damage
22636
Est Cost Emergency
452
Est Cost Environmental
10000
Est Cost Other
0
Prpty
33228
Accident Psig
7
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement. Release discovered by field personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Other
Int Visual Exam Details
Pinhole
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Elbow Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** S****
Preparer Title
Sr. Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2018-08-23 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On july 26, 2018 at 11:30 am cdt, pipeline maintenance crews discovered a release of approximately two barrels of crude on the tank 10 outgoing line at the superior terminal. A pinhole was discovered in the 6:00 position adjacent to the weld joining the 45 degree elbow to the pipe. As a precautionary measure, an nde analysis was completed on the second weld associated with the elbow and along the bottom of the pipe in the vicinity of the leak. No other defects or corrosion were observed. An 18 inch sleeve was welded to the pipe on july 27, 2018 and the line was returned to service. The cause of the release has been attributed to isolated internal corrosion. Approximately 150 tons of contaminated soil was disposed of at an approved site.
Report Received Date 2018-08-23 00:00:00
Iyear 2018
Report Number 20180250
Supplemental Number 30844
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2018-07-26 11:30:00
Location Latitude 46.686986 Google Maps OpenStreetMap
Location Longitude -92.057713 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-07-26 11:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Line Was Isolated
On Site Datetime 2018-07-26 11:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Superior Terminal
Segment Name Tank 10 Piping
Onshore State Abbreviation Wi
Onshore Postal Code 54880
Onshore City Name Superior
Onshore County Name Douglas
Designated Location Milepost/valve Station
Designated Name 1098
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 34
Pipe Wall Thickness 0.281
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Extruded Polyehylene
Weld Subtype Pipe Girth Weld
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 140
Est Cost Prop Damage 22636
Est Cost Emergency 452
Est Cost Environmental 10000
Est Cost Other 0
Prpty 33228
Accident Psig 7
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement. Release discovered by field personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Other
Int Visual Exam Details Pinhole
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Elbow Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** S****
Preparer Title Sr. Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2018-08-23 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On july 26, 2018 at 11:30 am cdt, pipeline maintenance crews discovered a release of approximately two barrels of crude on the tank 10 outgoing line at the superior terminal. A pinhole was discovered in the 6:00 position adjacent to the weld joining the 45 degree elbow to the pipe. As a precautionary measure, an nde analysis was completed on the second weld associated with the elbow and along the bottom of the pipe in the vicinity of the leak. No other defects or corrosion were observed. An 18 inch sleeve was welded to the pipe on july 27, 2018 and the line was returned to service. The cause of the release has been attributed to isolated internal corrosion. Approximately 150 tons of contaminated soil was disposed of at an approved site.

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