HL incident on 2018-07-23 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-07-23 11:30
Report number
Location
TX
Narrative
At approximately 1130 on 07/23/18, enterprise pipeline technician noticed the flow paddle on discharge side of pump began leaking into manifold. Approximately 2 barrels of mtbe leaked into concrete containment. Operation was shut down and leaking flow switch was isolated and removed. Normal operations restored. Clean up and remediation have been completed. Recurrence prevented by the removal of all similar flow switches at enterprise hsc facility.
Detailed record list
Report Received Date
2018-08-21 00:00:00
Iyear
2018
Report Number
20180247
Supplemental Number
31558
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-07-23 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Mtbe
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-07-23 11:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-07-23 11:35:00
Restart Datetime
2018-07-23 19:10:00
On Site Datetime
2018-07-23 11:30:00
Nrc Rpt Datetime
2018-07-23 13:20:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
D Manifold
Segment Name
Houston Ship Channel
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Dischg Pump
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
5000
Est Cost Other
0
Prpty
5150
Accident Psig
110
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were not a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Typical Wear And Tear
Preparer Name
D**** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
713-381-5647
Prepared Date
2019-01-28 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
713-381-5647
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
At approximately 1130 on 07/23/18, enterprise pipeline technician noticed the flow paddle on discharge side of pump began leaking into manifold. Approximately 2 barrels of mtbe leaked into concrete containment. Operation was shut down and leaking flow switch was isolated and removed. Normal operations restored. Clean up and remediation have been completed. Recurrence prevented by the removal of all similar flow switches at enterprise hsc facility.
Report Received Date 2018-08-21 00:00:00
Iyear 2018
Report Number 20180247
Supplemental Number 31558
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-07-23 11:30:00
Location Latitude 29.7435 Google Maps OpenStreetMap
Location Longitude -95.128 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Mtbe
Unintentional Release Bbls 2
Intentional Release Bbls 0
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-07-23 11:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-07-23 11:35:00
Restart Datetime 2018-07-23 19:10:00
On Site Datetime 2018-07-23 11:30:00
Nrc Rpt Datetime 2018-07-23 13:20:00
Nrc Rpt Num 1219267 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name D Manifold
Segment Name Houston Ship Channel
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Dischg Pump
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Instrumentation
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 5000
Est Cost Other 0
Prpty 5150
Accident Psig 110
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were not a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Typical Wear And Tear
Preparer Name D**** B*****
Preparer Title Pipeline Compliance Engineer
Preparer Email D*******@e****.com
Preparer Telephone 713-381-5647
Prepared Date 2019-01-28 00:00:00
Authorizer Name D**** B*****
Authorizer Telephone 713-381-5647
Authorizer Title Pipeline Compliance Engineer
Authorizer Email D*******@e****.com
Narrative At approximately 1130 on 07/23/18, enterprise pipeline technician noticed the flow paddle on discharge side of pump began leaking into manifold. Approximately 2 barrels of mtbe leaked into concrete containment. Operation was shut down and leaking flow switch was isolated and removed. Normal operations restored. Clean up and remediation have been completed. Recurrence prevented by the removal of all similar flow switches at enterprise hsc facility.

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