Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2018-07-12 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$3,000
Incident datetime
2018-07-12 01:05
Report number
Location
OK
Narrative
Operations personnel discovered a seal leak during inspection of the tank 368 mixers. Product movement into the tank was shut down. The release was contained and clean up activities commenced. The release occurred due to seal failure on the tank mixer. Product was transferred from the tank and the mixer seals were replaced. Approximately 10 cubic yards of soil were remediated.
Detailed record list
Report Received Date
2018-08-09 00:00:00
Iyear
2018
Report Number
20180233
Supplemental Number
30772
Report Type
Original Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-07-12 02:20:00
Location Latitude
29.747394
Location Longitude
-95.203336
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-07-12 01:05:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-07-12 01:05:00
Restart Datetime
2018-07-12 09:35:00
On Site Datetime
2018-07-12 01:05:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park
Segment Name
Terminal No. 474
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Not Within A Municipality
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
1980
Material Involved
Material Other Than Carbon Steel
Material Details
Mixer Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
110
Est Cost Prop Damage
3000
Est Cost Emergency
1500
Est Cost Environmental
0
Est Cost Other
0
Prpty
4610
Accident Psig
25
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Seal Failed Due To Normal Wear
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2018-08-09 00:00:00
Authorizer Name
M*** M*****
Authorizer Telephone
918-574-7073
Authorizer Title
Mgr Integrity Mgmt And Regulatory Compliance
Authorizer Email
M************@m*********.com
Narrative
Operations personnel discovered a seal leak during inspection of the tank 368 mixers. Product movement into the tank was shut down. The release was contained and clean up activities commenced. The release occurred due to seal failure on the tank mixer. Product was transferred from the tank and the mixer seals were replaced. Approximately 10 cubic yards of soil were remediated.
| Report Received Date | 2018-08-09 00:00:00 |
|---|---|
| Iyear | 2018 |
| Report Number | 20180233 |
| Supplemental Number | 30772 |
| Report Type | Original Final |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2018-07-12 02:20:00 |
| Location Latitude | 29.747394 Google Maps OpenStreetMap |
| Location Longitude | -95.203336 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 1 |
| Recovered Bbls | 1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2018-07-12 01:05:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2018-07-12 01:05:00 |
| Restart Datetime | 2018-07-12 09:35:00 |
| On Site Datetime | 2018-07-12 01:05:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Galena Park |
| Segment Name | Terminal No. 474 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77547 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Mixer |
| Tank Type | Atmospheric |
| Installation Year | 1980 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Mixer Seal |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 110 |
| Est Cost Prop Damage | 3000 |
| Est Cost Emergency | 1500 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 4610 |
| Accident Psig | 25 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Seal (Not Pump Seal) Or Packing |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Seal Failed Due To Normal Wear |
| Preparer Name | S****** L****** |
| Preparer Title | Ai Analyst |
| Preparer Email | S**************@m*********.com |
| Preparer Telephone | 918-574-7327 |
| Preparer Fax | 918-574-7376 |
| Prepared Date | 2018-08-09 00:00:00 |
| Authorizer Name | M*** M***** |
| Authorizer Telephone | 918-574-7073 |
| Authorizer Title | Mgr Integrity Mgmt And Regulatory Compliance |
| Authorizer Email | M************@m*********.com |
| Narrative | Operations personnel discovered a seal leak during inspection of the tank 368 mixers. Product movement into the tank was shut down. The release was contained and clean up activities commenced. The release occurred due to seal failure on the tank mixer. Product was transferred from the tank and the mixer seals were replaced. Approximately 10 cubic yards of soil were remediated. |
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