HL incident on 2018-07-10 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-07-10 12:27
Report number
Location
TX
Narrative
At 1227 houston control center (hcc) notified enterprise pipeline technicians of an lel alarm at lyssy station triggering a station shutdown. On site technicians were performing maintenance on the outbound 300 meter run and found a valve open that should have been closed during the maintenance activity. An open bleeder valve on top of the strainer basket allowed approximately 27 bbls of crude oil to be released. Investigation into the spill indicated the bleeder valve on top of the strainer was inadvertently locked open and should have been locked closed. This allowed crude oil to escape via the highpoint bleeder valve. No injuries were reported and the product was contained onsite without additional environmental impact. Technician oq's were suspended until retraining occurred.
Detailed record list
Report Received Date
2018-08-08 00:00:00
Iyear
2018
Report Number
20180232
Supplemental Number
37549
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-07-10 12:27:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
27
Recovered Bbls
27
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-07-10 12:27:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2018-07-10 07:45:00
Nrc Rpt Datetime
2018-07-10 13:38:00
Nrc Rpt Num
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lyssy Station
Segment Name
Meter Run
Onshore State Abbreviation
Tx
Onshore Postal Code
78113
Onshore City Name
Falls City
Onshore County Name
Wilson
Designated Location
Milepost
Designated Name
Lyssy Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Strainer Basket
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1600
Est Cost Prop Damage
0
Est Cost Emergency
24000
Est Cost Environmental
14000
Est Cost Other
1000
Est Cost Other Details
Miscellaneous
Prpty
40600
Accident Psig
5
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D**** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
713-381-5647
Prepared Date
2023-01-06 00:00:00
Authorizer Name
Y******* B**
Authorizer Telephone
713-381-5650
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
Y***@e****.com
Narrative
At 1227 houston control center (hcc) notified enterprise pipeline technicians of an lel alarm at lyssy station triggering a station shutdown. On site technicians were performing maintenance on the outbound 300 meter run and found a valve open that should have been closed during the maintenance activity. An open bleeder valve on top of the strainer basket allowed approximately 27 bbls of crude oil to be released. Investigation into the spill indicated the bleeder valve on top of the strainer was inadvertently locked open and should have been locked closed. This allowed crude oil to escape via the highpoint bleeder valve. No injuries were reported and the product was contained onsite without additional environmental impact. Technician oq's were suspended until retraining occurred.
Report Received Date 2018-08-08 00:00:00
Iyear 2018
Report Number 20180232
Supplemental Number 37549
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-07-10 12:27:00
Location Latitude 28.9226 Google Maps OpenStreetMap
Location Longitude -98.1435 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 27
Recovered Bbls 27
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-07-10 12:27:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
On Site Datetime 2018-07-10 07:45:00
Nrc Rpt Datetime 2018-07-10 13:38:00
Nrc Rpt Num 1217900 NRC Report How to search
Ignite Ind No
Num Pub Evacuated 0
Pipe Fac Name Lyssy Station
Segment Name Meter Run
Onshore State Abbreviation Tx
Onshore Postal Code 78113
Onshore City Name Falls City
Onshore County Name Wilson
Designated Location Milepost
Designated Name Lyssy Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Strainer Basket
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1600
Est Cost Prop Damage 0
Est Cost Emergency 24000
Est Cost Environmental 14000
Est Cost Other 1000
Est Cost Other Details Miscellaneous
Prpty 40600
Accident Psig 5
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D**** B*****
Preparer Title Pipeline Compliance Engineer
Preparer Email D*******@e****.com
Preparer Telephone 713-381-5647
Prepared Date 2023-01-06 00:00:00
Authorizer Name Y******* B**
Authorizer Telephone 713-381-5650
Authorizer Title Pipeline Compliance Engineer
Authorizer Email Y***@e****.com
Narrative At 1227 houston control center (hcc) notified enterprise pipeline technicians of an lel alarm at lyssy station triggering a station shutdown. On site technicians were performing maintenance on the outbound 300 meter run and found a valve open that should have been closed during the maintenance activity. An open bleeder valve on top of the strainer basket allowed approximately 27 bbls of crude oil to be released. Investigation into the spill indicated the bleeder valve on top of the strainer was inadvertently locked open and should have been locked closed. This allowed crude oil to escape via the highpoint bleeder valve. No injuries were reported and the product was contained onsite without additional environmental impact. Technician oq's were suspended until retraining occurred.

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