HL incident on 2018-07-05 — TX

Operator
Sunoco Pipeline L.p.
Cause
Notification Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2018-07-05 18:30
Report number
Location
TX
Narrative
On 07/05/18, a third party contractor was performing repairs to the tank dikes for separate operator at their facility adjacent to the 6/8" robert lee to jameson to colorado city pipeline row. The contractor was gathering soil with a backhoe for the dike repairs in the robert lee to jameson to colorado city pipeline row which resulted in striking the pipeline causing a release at approximately 18:30. After striking the pipeline, the contractor called the emergency number on the line marker to report the release to the houston control center. Upon notification the control center immediately shut down the pipeline and contacted local operations personnel. Upon arrival at approximately 19:00 operations personnel discovered an approximate release of 10 bbls of crude oil from the pipeline as a result of the 3rd party damage. Tx rrc was contacted at 20:16 and incident no. 1795 was assigned. All free product was recovered and approximately 2750 cubic yards of contaminated soil has been excavated and remediated on-site. Damaged section of pipe was cut out and replaced and line was restarted on 7/8/18 at 11:30. The contractor did not place a one-call notification prior to excavating soil on row. On 8/16/18 it was determined that environmental remediation costs would drive total costs for release over $50,000. Nrc was notified at 15:31 on 8/16/18 and report no. 1221762 was issued.
Detailed record list
Report Received Date
2018-08-04 00:00:00
Iyear
2018
Report Number
20180230
Supplemental Number
30813
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-07-05 18:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2018-07-05 18:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-07-05 18:35:00
Restart Datetime
2018-07-08 11:30:00
On Site Datetime
2018-07-05 19:00:00
Nrc Rpt Datetime
2018-08-16 15:31:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
6/8" Robert Lee To Jameson To Colorado City
Segment Name
633002
Onshore State Abbreviation
Tx
Onshore Postal Code
76945
Onshore City Name
Robert Lee
Onshore County Name
Coke
Designated Location
Milepost/valve Station
Designated Name
2230+39
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
16
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.156
Pipe Smys
24000
Pipe Specification
Api 5l
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1950
Manufactured Year
1950
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
0.5
Puncture Circum
1
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
650
Est Cost Prop Damage
40000
Est Cost Emergency
10000
Est Cost Environmental
70000
Est Cost Other
0
Prpty
120650
Accident Psig
178
Mop Psig
417
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
40000
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller reacted appropriately to call from excavator and immediately shutdown the pipeline and contacted local field operations personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
Yes
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Liquid Pipeline
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
65
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
T*** N*******
Preparer Title
Sr. Manager - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2018-08-16 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Sr. Manager - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 07/05/18, a third party contractor was performing repairs to the tank dikes for separate operator at their facility adjacent to the 6/8" robert lee to jameson to colorado city pipeline row. The contractor was gathering soil with a backhoe for the dike repairs in the robert lee to jameson to colorado city pipeline row which resulted in striking the pipeline causing a release at approximately 18:30. After striking the pipeline, the contractor called the emergency number on the line marker to report the release to the houston control center. Upon notification the control center immediately shut down the pipeline and contacted local operations personnel. Upon arrival at approximately 19:00 operations personnel discovered an approximate release of 10 bbls of crude oil from the pipeline as a result of the 3rd party damage. Tx rrc was contacted at 20:16 and incident no. 1795 was assigned. All free product was recovered and approximately 2750 cubic yards of contaminated soil has been excavated and remediated on-site. Damaged section of pipe was cut out and replaced and line was restarted on 7/8/18 at 11:30. The contractor did not place a one-call notification prior to excavating soil on row. On 8/16/18 it was determined that environmental remediation costs would drive total costs for release over $50,000. Nrc was notified at 15:31 on 8/16/18 and report no. 1221762 was issued.
Report Received Date 2018-08-04 00:00:00
Iyear 2018
Report Number 20180230
Supplemental Number 30813
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-07-05 18:30:00
Location Latitude 31.98165 Google Maps OpenStreetMap
Location Longitude -100.57514 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2018-07-05 18:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-07-05 18:35:00
Restart Datetime 2018-07-08 11:30:00
On Site Datetime 2018-07-05 19:00:00
Nrc Rpt Datetime 2018-08-16 15:31:00
Nrc Rpt Num 1221762 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 6/8" Robert Lee To Jameson To Colorado City
Segment Name 633002
Onshore State Abbreviation Tx
Onshore Postal Code 76945
Onshore City Name Robert Lee
Onshore County Name Coke
Designated Location Milepost/valve Station
Designated Name 2230+39
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 16
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.156
Pipe Smys 24000
Pipe Specification Api 5l
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1950
Manufactured Year 1950
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 0.5
Puncture Circum 1
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 650
Est Cost Prop Damage 40000
Est Cost Emergency 10000
Est Cost Environmental 70000
Est Cost Other 0
Prpty 120650
Accident Psig 178
Mop Psig 417
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 40000
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller reacted appropriately to call from excavator and immediately shutdown the pipeline and contacted local field operations personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt Yes
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Liquid Pipeline
One Call Notified Ind No
Service Interruption Yes
Service Interruption Hours 65
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name T*** N*******
Preparer Title Sr. Manager - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2018-08-16 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Sr. Manager - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 07/05/18, a third party contractor was performing repairs to the tank dikes for separate operator at their facility adjacent to the 6/8" robert lee to jameson to colorado city pipeline row. The contractor was gathering soil with a backhoe for the dike repairs in the robert lee to jameson to colorado city pipeline row which resulted in striking the pipeline causing a release at approximately 18:30. After striking the pipeline, the contractor called the emergency number on the line marker to report the release to the houston control center. Upon notification the control center immediately shut down the pipeline and contacted local operations personnel. Upon arrival at approximately 19:00 operations personnel discovered an approximate release of 10 bbls of crude oil from the pipeline as a result of the 3rd party damage. Tx rrc was contacted at 20:16 and incident no. 1795 was assigned. All free product was recovered and approximately 2750 cubic yards of contaminated soil has been excavated and remediated on-site. Damaged section of pipe was cut out and replaced and line was restarted on 7/8/18 at 11:30. The contractor did not place a one-call notification prior to excavating soil on row. On 8/16/18 it was determined that environmental remediation costs would drive total costs for release over $50,000. Nrc was notified at 15:31 on 8/16/18 and report no. 1221762 was issued.

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