Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2018-07-09 — OK
Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$6,500
Incident datetime
2018-07-09 13:15
Report number
Location
OK
Narrative
Filter vessel maintenance was performed oneok's silver creek injection site and the filter vessel brought back online on july 6th 2018. On july 9th at approximately 13:15 oneok contractors working at the site noticed an ice ball on the filter vessel door and contacted the local oneok pipeline operator. Operations personnel arrived on scene at approximately 13:48 and isolated the filter vessel. Product in the vessel and associated piping was then flared down. Prior to opening the vessel, nitrogen was used to purge the vessel of all combustibles. On 11 july, a maintenance crew steamed the vessel, removed and replaced the filter elements, and investigated the vessel to determine a cause of the release. The sealing element showed signs of tearing at the 11 o'clock position, which was determined to be the cause of the release. A representative of the vendor of the sealing element, used on the vessel door, was on site during the investigation and witnessed the installation of a new sealing element. The vessel was then returned to service. Initial communication from the oem representative indicated the sealing element had not been installed in the correct position. The oem representative stated the operator must verify the seal gland is smooth and use appropriate amounts of lithium grease so the sealing element is able move into the proper operating position during installation. As a result of a subsequent reportable accident (7/13/2018) and additional consultation with the oem, the oem determined the closure lids manufactured prior to 2009 were designed for a two piece sealing element which has been discontinued. In some cases these older closures could not successfully use the newer oem recommended one piece seal design due to the tolerance range of the closure lid during the initial milling. The oem is currently in the process of re-activating production of the original two piece sealing element design for operators with closure lids made prior to the design change in 2009. 18/08/08 - updated part c question 1 - pipeline is interstate per npms and annual report. Njones
Detailed record list
Report Received Date
2018-08-03 00:00:00
Iyear
2018
Report Number
20180227
Supplemental Number
30766
Report Type
Supplemental Final
Operator Id
32109
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-07-09 13:30:00
Location Latitude
32.808155
Location Longitude
-97.660138
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.14
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Operating Personnel
Incident Identified Datetime
2018-07-09 13:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Filter Vessel Isolated And By Passed, Pipeline Continued To Flow.
On Site Datetime
2018-07-09 13:48:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Crosstex Silver Creek Injection Site 536
Segment Name
Oneok Arbuckle Pipeline Index # 10484
Onshore State Abbreviation
Tx
Onshore Postal Code
76087
Onshore City Name
Not Within A Municipality
Onshore County Name
Parker
Designated Location
Milepost/valve Station
Designated Name
Inj. Site
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Pressure Vessel Head Or Wall
Installation Year
2008
Material Involved
Material Other Than Carbon Steel
Material Details
Sealing Element
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
6500
Est Cost Emergency
100
Est Cost Environmental
0
Est Cost Other
0
Prpty
6610
Accident Psig
803
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place prior to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Defect Ind
Yes
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Manager
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2018-08-08 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
N*********@o****.com
Narrative
Filter vessel maintenance was performed oneok's silver creek injection site and the filter vessel brought back online on july 6th 2018. On july 9th at approximately 13:15 oneok contractors working at the site noticed an ice ball on the filter vessel door and contacted the local oneok pipeline operator. Operations personnel arrived on scene at approximately 13:48 and isolated the filter vessel. Product in the vessel and associated piping was then flared down. Prior to opening the vessel, nitrogen was used to purge the vessel of all combustibles. On 11 july, a maintenance crew steamed the vessel, removed and replaced the filter elements, and investigated the vessel to determine a cause of the release. The sealing element showed signs of tearing at the 11 o'clock position, which was determined to be the cause of the release. A representative of the vendor of the sealing element, used on the vessel door, was on site during the investigation and witnessed the installation of a new sealing element. The vessel was then returned to service. Initial communication from the oem representative indicated the sealing element had not been installed in the correct position. The oem representative stated the operator must verify the seal gland is smooth and use appropriate amounts of lithium grease so the sealing element is able move into the proper operating position during installation. As a result of a subsequent reportable accident (7/13/2018) and additional consultation with the oem, the oem determined the closure lids manufactured prior to 2009 were designed for a two piece sealing element which has been discontinued. In some cases these older closures could not successfully use the newer oem recommended one piece seal design due to the tolerance range of the closure lid during the initial milling. The oem is currently in the process of re-activating production of the original two piece sealing element design for operators with closure lids made prior to the design change in 2009. 18/08/08 - updated part c question 1 - pipeline is interstate per npms and annual report. Njones
| Report Received Date | 2018-08-03 00:00:00 |
|---|---|
| Iyear | 2018 |
| Report Number | 20180227 |
| Supplemental Number | 30766 |
| Report Type | Supplemental Final |
| Operator Id | 32109 PHMSA Enforcement |
| Name | Oneok Ngl Pipeline, Llc |
| Operator Street Address | 100 West Fifth Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2018-07-09 13:30:00 |
| Location Latitude | 32.808155 Google Maps OpenStreetMap |
| Location Longitude | -97.660138 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
| Unintentional Release Bbls | 0.14 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Other |
| Accident Details | Third Party Operating Personnel |
| Incident Identified Datetime | 2018-07-09 13:15:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Filter Vessel Isolated And By Passed, Pipeline Continued To Flow. |
| On Site Datetime | 2018-07-09 13:48:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Crosstex Silver Creek Injection Site 536 |
| Segment Name | Oneok Arbuckle Pipeline Index # 10484 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 76087 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Parker |
| Designated Location | Milepost/valve Station |
| Designated Name | Inj. Site |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Pressure Vessel Head Or Wall |
| Installation Year | 2008 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Sealing Element |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Usa Ecological Ind | Yes |
| Usa Ecological Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 10 |
| Est Cost Prop Damage | 6500 |
| Est Cost Emergency | 100 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 6610 |
| Accident Psig | 803 |
| Mop Psig | 1440 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | No controller actions had taken place prior to the release. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Seal (Not Pump Seal) Or Packing |
| Additional Defect Ind | Yes |
| Preparer Name | N*** J**** |
| Preparer Title | Requlatory Compliance Manager |
| Preparer Email | N*********@o****.com |
| Preparer Telephone | 580-395-6304 |
| Preparer Fax | 580-395-2933 |
| Prepared Date | 2018-08-08 00:00:00 |
| Authorizer Name | N*** J**** |
| Authorizer Telephone | 580-395-6304 |
| Authorizer Title | Regulatory Compliance Manager |
| Authorizer Email | N*********@o****.com |
| Narrative | Filter vessel maintenance was performed oneok's silver creek injection site and the filter vessel brought back online on july 6th 2018. On july 9th at approximately 13:15 oneok contractors working at the site noticed an ice ball on the filter vessel door and contacted the local oneok pipeline operator. Operations personnel arrived on scene at approximately 13:48 and isolated the filter vessel. Product in the vessel and associated piping was then flared down. Prior to opening the vessel, nitrogen was used to purge the vessel of all combustibles. On 11 july, a maintenance crew steamed the vessel, removed and replaced the filter elements, and investigated the vessel to determine a cause of the release. The sealing element showed signs of tearing at the 11 o'clock position, which was determined to be the cause of the release. A representative of the vendor of the sealing element, used on the vessel door, was on site during the investigation and witnessed the installation of a new sealing element. The vessel was then returned to service. Initial communication from the oem representative indicated the sealing element had not been installed in the correct position. The oem representative stated the operator must verify the seal gland is smooth and use appropriate amounts of lithium grease so the sealing element is able move into the proper operating position during installation. As a result of a subsequent reportable accident (7/13/2018) and additional consultation with the oem, the oem determined the closure lids manufactured prior to 2009 were designed for a two piece sealing element which has been discontinued. In some cases these older closures could not successfully use the newer oem recommended one piece seal design due to the tolerance range of the closure lid during the initial milling. The oem is currently in the process of re-activating production of the original two piece sealing element design for operators with closure lids made prior to the design change in 2009. 18/08/08 - updated part c question 1 - pipeline is interstate per npms and annual report. Njones |
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