HL incident on 2018-06-27 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2018-06-27 05:01
Report number
Location
PA
Narrative
On wednesday, june 27, 2018 at 05:01 a.M., buckeye local operator received an lel alarm in the east chicago tank farm. Buckeye's local operator investigated the alarm and discovered the gasoline booster seal had failed shortly after the starting the unit. A controlled shut down of the pump was performed and the pump was isolated. All internal and external notifications were completed and the site was cleaned up by osro. The estimated release volume is 1 barrel of gasoline, all of which has been recovered. Buckeye technicians replaced the seal on june 28, 2018 and normal pipeline operations resumed on june 28, 2018 at 15:00. The root cause of the incident was determined to be equipment failure. The screws used for holding mechanical seal drive collar to pump shaft failed. The screws were replaced along with the seal.
Detailed record list
Report Received Date
2018-07-27 00:00:00
Iyear
2018
Report Number
20180216
Supplemental Number
31413
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2018-06-27 05:01:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Stationary Lel Detector
Incident Identified Datetime
2018-06-27 05:01:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-06-27 05:01:00
Restart Datetime
2018-06-28 15:00:00
On Site Datetime
2018-06-27 05:01:00
Nrc Rpt Datetime
2018-06-27 06:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
East Chicago Terminal
Segment Name
Tank Booster
Onshore State Abbreviation
In
Onshore Postal Code
46312
Onshore City Name
East Chicago
Onshore County Name
Lake County
Designated Location
Milepost/valve Station
Designated Name
East Chicago
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
5000
Est Cost Emergency
12000
Est Cost Environmental
0
Est Cost Other
0
Prpty
17000
Accident Psig
90
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The local operator was alerted by an lel monitor that is not in scada.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wrong Set Screws Used For Holding Mechanical Seal Drive Collar To Pump Shaft.
Preparer Name
C****** P********
Preparer Title
Director Regulatory Compliance
Preparer Email
C*********@b******.com
Preparer Telephone
610-904-4113
Prepared Date
2018-12-31 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On wednesday, june 27, 2018 at 05:01 a.M., buckeye local operator received an lel alarm in the east chicago tank farm. Buckeye's local operator investigated the alarm and discovered the gasoline booster seal had failed shortly after the starting the unit. A controlled shut down of the pump was performed and the pump was isolated. All internal and external notifications were completed and the site was cleaned up by osro. The estimated release volume is 1 barrel of gasoline, all of which has been recovered. Buckeye technicians replaced the seal on june 28, 2018 and normal pipeline operations resumed on june 28, 2018 at 15:00. The root cause of the incident was determined to be equipment failure. The screws used for holding mechanical seal drive collar to pump shaft failed. The screws were replaced along with the seal.
Report Received Date 2018-07-27 00:00:00
Iyear 2018
Report Number 20180216
Supplemental Number 31413
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2018-06-27 05:01:00
Location Latitude 41.64257 Google Maps OpenStreetMap
Location Longitude -87.466348 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Stationary Lel Detector
Incident Identified Datetime 2018-06-27 05:01:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-06-27 05:01:00
Restart Datetime 2018-06-28 15:00:00
On Site Datetime 2018-06-27 05:01:00
Nrc Rpt Datetime 2018-06-27 06:00:00
Nrc Rpt Num 1216555 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name East Chicago Terminal
Segment Name Tank Booster
Onshore State Abbreviation In
Onshore Postal Code 46312
Onshore City Name East Chicago
Onshore County Name Lake County
Designated Location Milepost/valve Station
Designated Name East Chicago
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 5000
Est Cost Emergency 12000
Est Cost Environmental 0
Est Cost Other 0
Prpty 17000
Accident Psig 90
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The local operator was alerted by an lel monitor that is not in scada.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Wrong Set Screws Used For Holding Mechanical Seal Drive Collar To Pump Shaft.
Preparer Name C****** P********
Preparer Title Director Regulatory Compliance
Preparer Email C*********@b******.com
Preparer Telephone 610-904-4113
Prepared Date 2018-12-31 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On wednesday, june 27, 2018 at 05:01 a.M., buckeye local operator received an lel alarm in the east chicago tank farm. Buckeye's local operator investigated the alarm and discovered the gasoline booster seal had failed shortly after the starting the unit. A controlled shut down of the pump was performed and the pump was isolated. All internal and external notifications were completed and the site was cleaned up by osro. The estimated release volume is 1 barrel of gasoline, all of which has been recovered. Buckeye technicians replaced the seal on june 28, 2018 and normal pipeline operations resumed on june 28, 2018 at 15:00. The root cause of the incident was determined to be equipment failure. The screws used for holding mechanical seal drive collar to pump shaft failed. The screws were replaced along with the seal.

All rights reserved. Copyright © by ClearPHMSA