HL incident on 2018-07-11 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2018-07-11 10:15
Report number
Location
OK
Narrative
While conducting a facility inspection, operations personnel discovered product dripping from the high discharge shutdown switch for the mainline unit. The unit and mainline were shutdown and clean up activities commenced. Impacted soil was containerized for proper disposal. The release originated from a faulty seal in the shutdown switch. The device was removed and replaced with a new shutdown switch. Approximately 1 cubic yard of soil was remediated
Detailed record list
Report Received Date
2018-07-26 00:00:00
Iyear
2018
Report Number
20180214
Supplemental Number
30699
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-07-11 10:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-07-11 10:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-07-11 10:25:00
Restart Datetime
2018-07-11 12:45:00
On Site Datetime
2018-07-11 10:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cheyenne Terminal
Segment Name
Terminal No. 419
Onshore State Abbreviation
Wy
Onshore Postal Code
82007
Onshore City Name
Cheyenne
Onshore County Name
Laramie
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Instrumentation
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Buna Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
100
Est Cost Emergency
200
Est Cost Environmental
0
Est Cost Other
200
Est Cost Other Details
Drum Shipment/disposal
Prpty
550
Accident Psig
785
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
All incident indications were below monitoring thresholds
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Defect Ind
Yes
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2018-07-26 00:00:00
Authorizer Name
M*** M******
Authorizer Telephone
(918) 574-7073
Authorizer Title
Mgr Integrity Mgmt And Regulatory Compliance
Authorizer Email
M***********@m*********.com
Narrative
While conducting a facility inspection, operations personnel discovered product dripping from the high discharge shutdown switch for the mainline unit. The unit and mainline were shutdown and clean up activities commenced. Impacted soil was containerized for proper disposal. The release originated from a faulty seal in the shutdown switch. The device was removed and replaced with a new shutdown switch. Approximately 1 cubic yard of soil was remediated
Report Received Date 2018-07-26 00:00:00
Iyear 2018
Report Number 20180214
Supplemental Number 30699
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2018-07-11 10:15:00
Location Latitude 41.10586 Google Maps OpenStreetMap
Location Longitude -104.833856 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-07-11 10:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-07-11 10:25:00
Restart Datetime 2018-07-11 12:45:00
On Site Datetime 2018-07-11 10:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cheyenne Terminal
Segment Name Terminal No. 419
Onshore State Abbreviation Wy
Onshore Postal Code 82007
Onshore City Name Cheyenne
Onshore County Name Laramie
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Instrumentation
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Buna Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 100
Est Cost Emergency 200
Est Cost Environmental 0
Est Cost Other 200
Est Cost Other Details Drum Shipment/disposal
Prpty 550
Accident Psig 785
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details All incident indications were below monitoring thresholds
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Defect Ind Yes
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2018-07-26 00:00:00
Authorizer Name M*** M******
Authorizer Telephone (918) 574-7073
Authorizer Title Mgr Integrity Mgmt And Regulatory Compliance
Authorizer Email M***********@m*********.com
Narrative While conducting a facility inspection, operations personnel discovered product dripping from the high discharge shutdown switch for the mainline unit. The unit and mainline were shutdown and clean up activities commenced. Impacted soil was containerized for proper disposal. The release originated from a faulty seal in the shutdown switch. The device was removed and replaced with a new shutdown switch. Approximately 1 cubic yard of soil was remediated

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