HL incident on 2018-06-27 — TX

Operator
Tesoro Socal Pipeline Company Llc
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-06-27 16:05
Report number
Location
TX
Narrative
On june 22nd, 2018 a pipeline leak was discovered near alameda st in the city of wilmington. A third party responded and cleaned up the incident shortly after discovery. The pipeline in question is inactive and contained a mixture of oily water. A mixture of oily water was recovered and approximately two barrels was crude oil. After the incident was cleaned up, the pipeline was drained down and temporarily repaired with a clamp, operators along the pipeline corridor were notified and responded at the site. Cause investigation and verification of ownership are still being conducted by andeavor. We are waiting for permits with the port of long beach and port of los angeles to conduct field work to investigate cause, confirm ownership and permanently repair. A supplemental nrc report, 1216840, was called in on 6/29/2018 at 14:34 local time to update the spill volume from 68 barrels of crude spilled to 68 barrels of crude/water mix for a total of 2 barrels of crude spilled. Update 8/20/18: we have confirmed that this incident involved tesoro socal pipeline's line e-51h. We have obtained permits with the polb and pola and will be removing the pipeline. Project planning has started, field work is estimated to begin mid september. We will begin investigation on the cause and an update will be provided. Update 1/22/2019: rca was completed on 1/03/19. We are waiting for permits from the polb and pola to go to the field to inspect the pipeline and properly abandon it. Update 10/18/2021: at this time we are still waiting for permits to be provided by polb and pola to properly abandon / remove this portion of line. It is presumed that internal corrosion was present at the location of the leak and the report will be closed. Please note section e question 5, a and b ask what type of valve initially isolated the pipe up and downstream of the leak. This line is abandoned, cut, and capped physically isolated from any active segment. Manual valve was selected since there was no other option.
Detailed record list
Report Received Date
2018-07-20 00:00:00
Iyear
2018
Report Number
20180209
Supplemental Number
35892
Report Type
Supplemental Final
Operator Id
Name
Tesoro Socal Pipeline Company Llc
Operator Street Address
19100 Ridgewood Parkway
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78259
Local Datetime
2018-06-22 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Another Operator
Incident Identified Datetime
2018-06-27 16:05:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Not Active.
On Site Datetime
2018-06-27 16:05:00
Nrc Rpt Datetime
2018-06-27 16:46:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Line E51
Segment Name
Segment H
Onshore State Abbreviation
Ca
Onshore Postal Code
90744
Onshore City Name
Wilmington
Onshore County Name
Los Angeles
Designated Location
Milepost/valve Station
Designated Name
.57 Miles
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Unknown
Installation Year
1970
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Unknown
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
7000
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
62000
Est Cost Environmental
0
Est Cost Other
0
Prpty
69000
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
No
Unsuitable Mainline Ind
Yes
Tight Mitered Ind
Yes
Other Restrictions Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
No Launching And Receiving Facilities.
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name
A*** R*********
Preparer Title
Hes Professional
Preparer Email
A***********@m****************.com
Preparer Telephone
7146422245
Prepared Date
2021-10-18 00:00:00
Authorizer Name
A**** M*******
Authorizer Telephone
2106266343
Authorizer Title
Environmental Safety And Security Manager
Authorizer Email
A*********@m****************.com
Narrative
On june 22nd, 2018 a pipeline leak was discovered near alameda st in the city of wilmington. A third party responded and cleaned up the incident shortly after discovery. The pipeline in question is inactive and contained a mixture of oily water. A mixture of oily water was recovered and approximately two barrels was crude oil. After the incident was cleaned up, the pipeline was drained down and temporarily repaired with a clamp, operators along the pipeline corridor were notified and responded at the site. Cause investigation and verification of ownership are still being conducted by andeavor. We are waiting for permits with the port of long beach and port of los angeles to conduct field work to investigate cause, confirm ownership and permanently repair. A supplemental nrc report, 1216840, was called in on 6/29/2018 at 14:34 local time to update the spill volume from 68 barrels of crude spilled to 68 barrels of crude/water mix for a total of 2 barrels of crude spilled. Update 8/20/18: we have confirmed that this incident involved tesoro socal pipeline's line e-51h. We have obtained permits with the polb and pola and will be removing the pipeline. Project planning has started, field work is estimated to begin mid september. We will begin investigation on the cause and an update will be provided. Update 1/22/2019: rca was completed on 1/03/19. We are waiting for permits from the polb and pola to go to the field to inspect the pipeline and properly abandon it. Update 10/18/2021: at this time we are still waiting for permits to be provided by polb and pola to properly abandon / remove this portion of line. It is presumed that internal corrosion was present at the location of the leak and the report will be closed. Please note section e question 5, a and b ask what type of valve initially isolated the pipe up and downstream of the leak. This line is abandoned, cut, and capped physically isolated from any active segment. Manual valve was selected since there was no other option.
Report Received Date 2018-07-20 00:00:00
Iyear 2018
Report Number 20180209
Supplemental Number 35892
Report Type Supplemental Final
Operator Id 39013 PHMSA Enforcement
Name Tesoro Socal Pipeline Company Llc
Operator Street Address 19100 Ridgewood Parkway
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78259
Local Datetime 2018-06-22 13:00:00
Location Latitude 33.78269 Google Maps OpenStreetMap
Location Longitude -118.24431 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Another Operator
Incident Identified Datetime 2018-06-27 16:05:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Not Active.
On Site Datetime 2018-06-27 16:05:00
Nrc Rpt Datetime 2018-06-27 16:46:00
Nrc Rpt Num 1216633 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Line E51
Segment Name Segment H
Onshore State Abbreviation Ca
Onshore Postal Code 90744
Onshore City Name Wilmington
Onshore County Name Los Angeles
Designated Location Milepost/valve Station
Designated Name .57 Miles
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Unknown
Installation Year 1970
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Unknown
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 7000
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 62000
Est Cost Environmental 0
Est Cost Other 0
Prpty 69000
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind No
Unsuitable Mainline Ind Yes
Tight Mitered Ind Yes
Other Restrictions Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details No Launching And Receiving Facilities.
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name A*** R*********
Preparer Title Hes Professional
Preparer Email A***********@m****************.com
Preparer Telephone 7146422245
Prepared Date 2021-10-18 00:00:00
Authorizer Name A**** M*******
Authorizer Telephone 2106266343
Authorizer Title Environmental Safety And Security Manager
Authorizer Email A*********@m****************.com
Narrative On june 22nd, 2018 a pipeline leak was discovered near alameda st in the city of wilmington. A third party responded and cleaned up the incident shortly after discovery. The pipeline in question is inactive and contained a mixture of oily water. A mixture of oily water was recovered and approximately two barrels was crude oil. After the incident was cleaned up, the pipeline was drained down and temporarily repaired with a clamp, operators along the pipeline corridor were notified and responded at the site. Cause investigation and verification of ownership are still being conducted by andeavor. We are waiting for permits with the port of long beach and port of los angeles to conduct field work to investigate cause, confirm ownership and permanently repair. A supplemental nrc report, 1216840, was called in on 6/29/2018 at 14:34 local time to update the spill volume from 68 barrels of crude spilled to 68 barrels of crude/water mix for a total of 2 barrels of crude spilled. Update 8/20/18: we have confirmed that this incident involved tesoro socal pipeline's line e-51h. We have obtained permits with the polb and pola and will be removing the pipeline. Project planning has started, field work is estimated to begin mid september. We will begin investigation on the cause and an update will be provided. Update 1/22/2019: rca was completed on 1/03/19. We are waiting for permits from the polb and pola to go to the field to inspect the pipeline and properly abandon it. Update 10/18/2021: at this time we are still waiting for permits to be provided by polb and pola to properly abandon / remove this portion of line. It is presumed that internal corrosion was present at the location of the leak and the report will be closed. Please note section e question 5, a and b ask what type of valve initially isolated the pipe up and downstream of the leak. This line is abandoned, cut, and capped physically isolated from any active segment. Manual valve was selected since there was no other option.

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