HL incident on 2018-06-19 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-06-19 12:30
Report number
Location
OK
Narrative
A flash fire occurred on june 19, 2018, at the oneok ngl pipeline, sterling iii groveton pump station while personnel were welding a flange on pump header piping during construction/maintenance work. The fire was immediately extinguished and there were no injuries. The pump station piping had been isolated (air gapped); products evacuated, nitrogen purged, and then left open to atmosphere for 24 hours prior to the beginning of the work. During the course of the work, crews had cut the piping going to the pump and had successfully installed the first flange. The fire occurred during the installation of the second flange on the same piping. The fire immediately burned itself out, and the fire watch discharged a fire extinguisher. The incident occurred simultaneously with valve maintenance activity that was occurring in close proximity. The pipe had been evacuated and, as an additional precaution, hydrocarbon monitoring was in place both upstream and downstream of the valve work, without any hydrocarbon detection. However, the addition of the valve work may have resulted in undetected hydrocarbons impacting the welding operation. After the incident, all work was stopped and the work procedures were reviewed. The hot work was terminated until the valve maintenance was completed. Upon completion of the valve work, the area was verified to be hydrocarbon free, and the welding was completed without incident. As a result of the incident, oneok has re-emphasized the hazards of simultaneous work and is reviewing future scheduled work activities in order to better manage the hazards associated with simultaneous work. Updated 8/20/18: updated number of company employees drug tested to 6. Zero test failures.
Detailed record list
Report Received Date
2018-07-19 00:00:00
Iyear
2018
Report Number
20180207
Supplemental Number
30822
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-06-19 12:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.02
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-06-19 12:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Facility Was Isolated And Shutdown Previously To Release
On Site Datetime
2018-06-19 12:30:00
Nrc Rpt Datetime
2018-06-22 11:16:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Groveton Pump Station
Segment Name
Oneok Sterling Iii Pipeline Index #10547
Onshore State Abbreviation
Tx
Onshore Postal Code
75845
Onshore City Name
Not Within A Municipality
Onshore County Name
Trinity
Designated Location
Survey Station No.
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Flash Fire From Residual Gas While Welding A Flange To Station Piping.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
50
Est Cost Environmental
0
Est Cost Other
0
Prpty
50
Accident Psig
0
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place. Pump station was isolated from pipeline and shutdown. Station was under local control.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
6
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Multiple Construction And Maintenance Tasks Were Occurring Simultaneously At The Pump Station. Station Had Been Air Gapped Nitrogen Purged And Hydrocarbons Vented For More Than 24 Hours. The Addition Of The Valve Work While Conducting Hot Work May Have Resulted In Undetected Hydrocarbons Impacting The Welding.
Related Inadequate Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Manager
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2018-08-20 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
N*********@o****.com
Narrative
A flash fire occurred on june 19, 2018, at the oneok ngl pipeline, sterling iii groveton pump station while personnel were welding a flange on pump header piping during construction/maintenance work. The fire was immediately extinguished and there were no injuries. The pump station piping had been isolated (air gapped); products evacuated, nitrogen purged, and then left open to atmosphere for 24 hours prior to the beginning of the work. During the course of the work, crews had cut the piping going to the pump and had successfully installed the first flange. The fire occurred during the installation of the second flange on the same piping. The fire immediately burned itself out, and the fire watch discharged a fire extinguisher. The incident occurred simultaneously with valve maintenance activity that was occurring in close proximity. The pipe had been evacuated and, as an additional precaution, hydrocarbon monitoring was in place both upstream and downstream of the valve work, without any hydrocarbon detection. However, the addition of the valve work may have resulted in undetected hydrocarbons impacting the welding operation. After the incident, all work was stopped and the work procedures were reviewed. The hot work was terminated until the valve maintenance was completed. Upon completion of the valve work, the area was verified to be hydrocarbon free, and the welding was completed without incident. As a result of the incident, oneok has re-emphasized the hazards of simultaneous work and is reviewing future scheduled work activities in order to better manage the hazards associated with simultaneous work. Updated 8/20/18: updated number of company employees drug tested to 6. Zero test failures.
Report Received Date 2018-07-19 00:00:00
Iyear 2018
Report Number 20180207
Supplemental Number 30822
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2018-06-19 12:30:00
Location Latitude 31.0525 Google Maps OpenStreetMap
Location Longitude -95.2443 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.02
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-06-19 12:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Facility Was Isolated And Shutdown Previously To Release
On Site Datetime 2018-06-19 12:30:00
Nrc Rpt Datetime 2018-06-22 11:16:00
Nrc Rpt Num 1216109 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Groveton Pump Station
Segment Name Oneok Sterling Iii Pipeline Index #10547
Onshore State Abbreviation Tx
Onshore Postal Code 75845
Onshore City Name Not Within A Municipality
Onshore County Name Trinity
Designated Location Survey Station No.
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2018
Material Involved Carbon Steel
Release Type Other
Release Type Details Flash Fire From Residual Gas While Welding A Flange To Station Piping.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 50
Est Cost Environmental 0
Est Cost Other 0
Prpty 50
Accident Psig 0
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place. Pump station was isolated from pipeline and shutdown. Station was under local control.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 6
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Multiple Construction And Maintenance Tasks Were Occurring Simultaneously At The Pump Station. Station Had Been Air Gapped Nitrogen Purged And Hydrocarbons Vented For More Than 24 Hours. The Addition Of The Valve Work While Conducting Hot Work May Have Resulted In Undetected Hydrocarbons Impacting The Welding.
Related Inadequate Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name N*** J****
Preparer Title Requlatory Compliance Manager
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2018-08-20 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Manager
Authorizer Email N*********@o****.com
Narrative A flash fire occurred on june 19, 2018, at the oneok ngl pipeline, sterling iii groveton pump station while personnel were welding a flange on pump header piping during construction/maintenance work. The fire was immediately extinguished and there were no injuries. The pump station piping had been isolated (air gapped); products evacuated, nitrogen purged, and then left open to atmosphere for 24 hours prior to the beginning of the work. During the course of the work, crews had cut the piping going to the pump and had successfully installed the first flange. The fire occurred during the installation of the second flange on the same piping. The fire immediately burned itself out, and the fire watch discharged a fire extinguisher. The incident occurred simultaneously with valve maintenance activity that was occurring in close proximity. The pipe had been evacuated and, as an additional precaution, hydrocarbon monitoring was in place both upstream and downstream of the valve work, without any hydrocarbon detection. However, the addition of the valve work may have resulted in undetected hydrocarbons impacting the welding operation. After the incident, all work was stopped and the work procedures were reviewed. The hot work was terminated until the valve maintenance was completed. Upon completion of the valve work, the area was verified to be hydrocarbon free, and the welding was completed without incident. As a result of the incident, oneok has re-emphasized the hazards of simultaneous work and is reviewing future scheduled work activities in order to better manage the hazards associated with simultaneous work. Updated 8/20/18: updated number of company employees drug tested to 6. Zero test failures.

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