HL incident on 2018-06-11 — TX

Operator
Genesis Pipeline Texas, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-06-11 15:03
Report number
Location
TX
Narrative
While conducting a facility walk-through, a 3rd party representative noticed product coming out of the tank 111 mixer motor at the webster station in texas. The contractor notified his supervisor which then notified genesis personnel of the leak. Genesis personnel immediately responded to find product leaking into secondary containment area in which boom was spread to help contain crude oil within the tank secondary containment area. Containment pans were also placed at the source to prevent product from reaching the ground while osro was en route. The tank mixer was repaired in-house and the leak was stopped at 18:30 on the same day. The liquid product/contaminated soil was picked up and removed by osro. In total, approximately 60 gallons of crude oil leaked from the mixer seal with approximately 20 gallons reaching the ground. All product was contained inside the tank's secondary containment area. Note: part e, question 2 - form required data for this question although accident occurred at tank mixer. Genesis used the mop for an 18" pipeline feeding this tank. Part e, question 5f - form required data for this question although "no" was automatically filled in by system for question 5. Genesis used an 18" pipeline feeding this tank to answer this question. Supplemental update (8/21/18) - revision of part d question 7. Added "yes" to "high population" hca and "other population" hca to reflect records.
Detailed record list
Report Received Date
2018-07-06 00:00:00
Iyear
2018
Report Number
20180193
Supplemental Number
30832
Report Type
Supplemental Final
Operator Id
Name
Genesis Pipeline Texas, L.p.
Operator Street Address
811 Louisiana St. Suite 1200
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002-5417
Local Datetime
2018-06-11 15:03:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.42
Recovered Bbls
1.42
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-06-11 15:03:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank 111 Has Been Static For Several Months.
On Site Datetime
2018-06-11 15:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Webster Station
Segment Name
Tank 111
Onshore State Abbreviation
Tx
Onshore Postal Code
77598
Onshore City Name
Webster
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Webster
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Seal On Mixer
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
4200
Est Cost Prop Damage
0
Est Cost Emergency
7500
Est Cost Environmental
0
Est Cost Other
0
Prpty
11700
Accident Psig
20
Mop Psig
1140
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Slow leak on tank seal mixer.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Vibration Ind
Yes
Additional Defect Ind
Yes
Preparer Name
J**** M*****
Preparer Title
Pipeline Compliance Specialist
Preparer Email
J***********@g****.com
Preparer Telephone
225-263-0575
Prepared Date
2018-08-21 00:00:00
Authorizer Name
J*** J*****
Authorizer Telephone
713-860-2605
Authorizer Title
Dot Compliance Manager
Authorizer Email
J**********@g****.com
Narrative
While conducting a facility walk-through, a 3rd party representative noticed product coming out of the tank 111 mixer motor at the webster station in texas. The contractor notified his supervisor which then notified genesis personnel of the leak. Genesis personnel immediately responded to find product leaking into secondary containment area in which boom was spread to help contain crude oil within the tank secondary containment area. Containment pans were also placed at the source to prevent product from reaching the ground while osro was en route. The tank mixer was repaired in-house and the leak was stopped at 18:30 on the same day. The liquid product/contaminated soil was picked up and removed by osro. In total, approximately 60 gallons of crude oil leaked from the mixer seal with approximately 20 gallons reaching the ground. All product was contained inside the tank's secondary containment area. Note: part e, question 2 - form required data for this question although accident occurred at tank mixer. Genesis used the mop for an 18" pipeline feeding this tank. Part e, question 5f - form required data for this question although "no" was automatically filled in by system for question 5. Genesis used an 18" pipeline feeding this tank to answer this question. Supplemental update (8/21/18) - revision of part d question 7. Added "yes" to "high population" hca and "other population" hca to reflect records.
Report Received Date 2018-07-06 00:00:00
Iyear 2018
Report Number 20180193
Supplemental Number 30832
Report Type Supplemental Final
Operator Id 32407 PHMSA Enforcement
Name Genesis Pipeline Texas, L.p.
Operator Street Address 811 Louisiana St. Suite 1200
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002-5417
Local Datetime 2018-06-11 15:03:00
Location Latitude 29.524865 Google Maps OpenStreetMap
Location Longitude -95.107522 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.42
Recovered Bbls 1.42
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-06-11 15:03:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank 111 Has Been Static For Several Months.
On Site Datetime 2018-06-11 15:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Webster Station
Segment Name Tank 111
Onshore State Abbreviation Tx
Onshore Postal Code 77598
Onshore City Name Webster
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Webster
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Seal On Mixer
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 4200
Est Cost Prop Damage 0
Est Cost Emergency 7500
Est Cost Environmental 0
Est Cost Other 0
Prpty 11700
Accident Psig 20
Mop Psig 1140
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Slow leak on tank seal mixer.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Vibration Ind Yes
Additional Defect Ind Yes
Preparer Name J**** M*****
Preparer Title Pipeline Compliance Specialist
Preparer Email J***********@g****.com
Preparer Telephone 225-263-0575
Prepared Date 2018-08-21 00:00:00
Authorizer Name J*** J*****
Authorizer Telephone 713-860-2605
Authorizer Title Dot Compliance Manager
Authorizer Email J**********@g****.com
Narrative While conducting a facility walk-through, a 3rd party representative noticed product coming out of the tank 111 mixer motor at the webster station in texas. The contractor notified his supervisor which then notified genesis personnel of the leak. Genesis personnel immediately responded to find product leaking into secondary containment area in which boom was spread to help contain crude oil within the tank secondary containment area. Containment pans were also placed at the source to prevent product from reaching the ground while osro was en route. The tank mixer was repaired in-house and the leak was stopped at 18:30 on the same day. The liquid product/contaminated soil was picked up and removed by osro. In total, approximately 60 gallons of crude oil leaked from the mixer seal with approximately 20 gallons reaching the ground. All product was contained inside the tank's secondary containment area. Note: part e, question 2 - form required data for this question although accident occurred at tank mixer. Genesis used the mop for an 18" pipeline feeding this tank. Part e, question 5f - form required data for this question although "no" was automatically filled in by system for question 5. Genesis used an 18" pipeline feeding this tank to answer this question. Supplemental update (8/21/18) - revision of part d question 7. Added "yes" to "high population" hca and "other population" hca to reflect records.

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