HL incident on 2018-06-04 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2018-06-04 21:15
Report number
Location
PA
Narrative
At approximately 21:15 on june 4, 2018, buckeye personnel identified that motor operated valve (mov) 892 belonging to 16" pp861hf (viking) had leaked approximately 4 gallons of crude at the northwest corner of buckeye texas processing (btp) facility. At this time, buckeye personnel implemented containment measures under mov 892 and ensured that the valve was no longer actively leaking before making the appropriate internal notifications. At approximately 23:15, a telephonic release notification was made to the railroad commission of texas and it was reported that approximately 4 gallons of product had contaminated the soil. At approximately 7:40 on june 5, 2018, a contractor arrived on-site, tightened the packing on mov 892, and permanently stopped the leak. At this time it was identified that an additional 31 gallons of crude had leaked into the newly implemented containment under mov 892. The leak was confined to buckeye owned property and all remediation activities have been completed. There were no injuries or deaths; no ignition of the commodity released; traffic did not need to be re-routed; no media was involved; and all required notifications were made. The root cause of the crude release has been attributed to the breakdown of the packing in mov 892, which will continue to be monitored during mainline valve inspections every 6 months, not to exceed 7 1/2 months.
Detailed record list
Report Received Date
2018-06-29 00:00:00
Iyear
2018
Report Number
20180184
Supplemental Number
30779
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2018-06-04 21:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.7
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-06-04 21:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Not Actively Flowing Product At The Time Of Discovery.
On Site Datetime
2018-06-04 21:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Pp861hf
Segment Name
16" Viking
Onshore State Abbreviation
Tx
Onshore Postal Code
78409
Onshore City Name
Corpus Christi
Onshore County Name
Nueces
Designated Location
Milepost/valve Station
Designated Name
Btp Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Other
Valve Mainline Details
Motor Operated Valve
Valve Manufacturer
Walworth
Installation Year
2018
Manufactured Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
46
Est Cost Prop Damage
1500
Est Cost Emergency
1494
Est Cost Environmental
0
Est Cost Other
0
Prpty
3040
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline system was not actively moving product when the release was identified.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Breakdown Of Packing
Preparer Name
V****** G**************
Preparer Title
District Compliance Specialist
Preparer Email
V***************@b******.com
Preparer Telephone
361-792-3083
Prepared Date
2018-08-10 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4916
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
At approximately 21:15 on june 4, 2018, buckeye personnel identified that motor operated valve (mov) 892 belonging to 16" pp861hf (viking) had leaked approximately 4 gallons of crude at the northwest corner of buckeye texas processing (btp) facility. At this time, buckeye personnel implemented containment measures under mov 892 and ensured that the valve was no longer actively leaking before making the appropriate internal notifications. At approximately 23:15, a telephonic release notification was made to the railroad commission of texas and it was reported that approximately 4 gallons of product had contaminated the soil. At approximately 7:40 on june 5, 2018, a contractor arrived on-site, tightened the packing on mov 892, and permanently stopped the leak. At this time it was identified that an additional 31 gallons of crude had leaked into the newly implemented containment under mov 892. The leak was confined to buckeye owned property and all remediation activities have been completed. There were no injuries or deaths; no ignition of the commodity released; traffic did not need to be re-routed; no media was involved; and all required notifications were made. The root cause of the crude release has been attributed to the breakdown of the packing in mov 892, which will continue to be monitored during mainline valve inspections every 6 months, not to exceed 7 1/2 months.
Report Received Date 2018-06-29 00:00:00
Iyear 2018
Report Number 20180184
Supplemental Number 30779
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2018-06-04 21:15:00
Location Latitude 27.8189044 Google Maps OpenStreetMap
Location Longitude -97.5079139 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.7
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-06-04 21:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Not Actively Flowing Product At The Time Of Discovery.
On Site Datetime 2018-06-04 21:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Pp861hf
Segment Name 16" Viking
Onshore State Abbreviation Tx
Onshore Postal Code 78409
Onshore City Name Corpus Christi
Onshore County Name Nueces
Designated Location Milepost/valve Station
Designated Name Btp Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Other
Valve Mainline Details Motor Operated Valve
Valve Manufacturer Walworth
Installation Year 2018
Manufactured Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 46
Est Cost Prop Damage 1500
Est Cost Emergency 1494
Est Cost Environmental 0
Est Cost Other 0
Prpty 3040
Accident Psig 0
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline system was not actively moving product when the release was identified.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Breakdown Of Packing
Preparer Name V****** G**************
Preparer Title District Compliance Specialist
Preparer Email V***************@b******.com
Preparer Telephone 361-792-3083
Prepared Date 2018-08-10 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4916
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative At approximately 21:15 on june 4, 2018, buckeye personnel identified that motor operated valve (mov) 892 belonging to 16" pp861hf (viking) had leaked approximately 4 gallons of crude at the northwest corner of buckeye texas processing (btp) facility. At this time, buckeye personnel implemented containment measures under mov 892 and ensured that the valve was no longer actively leaking before making the appropriate internal notifications. At approximately 23:15, a telephonic release notification was made to the railroad commission of texas and it was reported that approximately 4 gallons of product had contaminated the soil. At approximately 7:40 on june 5, 2018, a contractor arrived on-site, tightened the packing on mov 892, and permanently stopped the leak. At this time it was identified that an additional 31 gallons of crude had leaked into the newly implemented containment under mov 892. The leak was confined to buckeye owned property and all remediation activities have been completed. There were no injuries or deaths; no ignition of the commodity released; traffic did not need to be re-routed; no media was involved; and all required notifications were made. The root cause of the crude release has been attributed to the breakdown of the packing in mov 892, which will continue to be monitored during mainline valve inspections every 6 months, not to exceed 7 1/2 months.

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