HL incident on 2018-06-01 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,100
Incident datetime
2018-06-01 19:20
Report number
Location
TX
Narrative
On 6/1/2018, usld was observed in containment at pasadena terminal's gp manifold. Upon investigation, it was discovered that the thermal pressure relief valve was popping off to relief thermal pressure but failed to seat properly. As the product filled the sump, the pump to remove product failed to engage which caused product to overflow unto containment. Product was removed via vacuum truck and the thermal relief valve replaced. Corrective actions: all discharge from relief valves are being piped directly into a transmix tank to prevent this from reoccurring.
Detailed record list
Report Received Date
2018-06-28 00:00:00
Iyear
2018
Report Number
20180182
Supplemental Number
30856
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-06-01 19:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
107
Recovered Bbls
107
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-06-01 19:20:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Shutdown Prior To Accident
On Site Datetime
2018-06-01 19:20:00
Nrc Rpt Datetime
2018-06-01 22:49:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pasadena Terminal
Segment Name
20-Pl-36000
Onshore State Abbreviation
Tx
Onshore Postal Code
77506-0351
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Spring In Thermal Relief Valve Failed To Seat
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
2100
Est Cost Emergency
150
Est Cost Environmental
0
Est Cost Other
20000
Est Cost Other Details
New Pipe Connection From Prv To Tank 15-1
Prpty
22250
Accident Psig
3
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Equipment failure, not caused by controller
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Thermal Relief Valve Seat Failed To Engage Properly
Preparer Name
D******* S*******
Preparer Title
Director Of Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
713-420-6496
Preparer Fax
303-984-3048
Prepared Date
2018-08-24 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713-420-6496
Authorizer Title
Director Of Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 6/1/2018, usld was observed in containment at pasadena terminal's gp manifold. Upon investigation, it was discovered that the thermal pressure relief valve was popping off to relief thermal pressure but failed to seat properly. As the product filled the sump, the pump to remove product failed to engage which caused product to overflow unto containment. Product was removed via vacuum truck and the thermal relief valve replaced. Corrective actions: all discharge from relief valves are being piped directly into a transmix tank to prevent this from reoccurring.
Report Received Date 2018-06-28 00:00:00
Iyear 2018
Report Number 20180182
Supplemental Number 30856
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-06-01 19:20:00
Location Latitude 29.72536 Google Maps OpenStreetMap
Location Longitude -95.20334 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 107
Recovered Bbls 107
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-06-01 19:20:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Shutdown Prior To Accident
On Site Datetime 2018-06-01 19:20:00
Nrc Rpt Datetime 2018-06-01 22:49:00
Nrc Rpt Num 1213959 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pasadena Terminal
Segment Name 20-Pl-36000
Onshore State Abbreviation Tx
Onshore Postal Code 77506-0351
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Installation Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Spring In Thermal Relief Valve Failed To Seat
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 2100
Est Cost Emergency 150
Est Cost Environmental 0
Est Cost Other 20000
Est Cost Other Details New Pipe Connection From Prv To Tank 15-1
Prpty 22250
Accident Psig 3
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Equipment failure, not caused by controller
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Thermal Relief Valve Seat Failed To Engage Properly
Preparer Name D******* S*******
Preparer Title Director Of Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 713-420-6496
Preparer Fax 303-984-3048
Prepared Date 2018-08-24 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713-420-6496
Authorizer Title Director Of Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 6/1/2018, usld was observed in containment at pasadena terminal's gp manifold. Upon investigation, it was discovered that the thermal pressure relief valve was popping off to relief thermal pressure but failed to seat properly. As the product filled the sump, the pump to remove product failed to engage which caused product to overflow unto containment. Product was removed via vacuum truck and the thermal relief valve replaced. Corrective actions: all discharge from relief valves are being piped directly into a transmix tank to prevent this from reoccurring.

All rights reserved. Copyright © by ClearPHMSA