HL incident on 2018-06-11 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$140,915
Incident datetime
2018-06-11 08:00
Report number
Location
GA
Narrative
On 6/11/18 at 0800 est, a contract inspector notified the belton lead technician of a stem seal leak on the danielsville station suction valve. After initial notifications, the contract inspector was able to contain the leaking product. The lead technician immediately notified the control center and the lead operator. The lead technician dispatched technician to facility to make repairs and start recovery of spilled product. The lead operator contacted the manager of operations at 0827 est. Director of operations was notified at 0838 and district environmental was notified at 0843 by manager of operations. By 0920, the technician was able to install tubing from the suction valve yoke tube directly to the station sump isolating the leak source as a temporary repair. Contract crews and the district environmental specialist arrived on site at 1130 to assist in recovery. Remedial actions included excavation of contaminated soil and vacuum recovery of any free standing product. On 6/12/18 at 0924 est nrc notification was made when it was determined that the $50,000 notification threshold would be exceeded. Concurrently, a courtesy notification was also made to ga dnr epd - natural recourses operations center and the ga epd case manager for the existing remediation site at the facility. The current estimated release volume is 375 gallons based on estimated time of release and observed rate of release. Final volume of release and recovery will be communicated once excavation is complete and analytical analyses are available. Currently, 80 tons of soil have been excavated and calculated to contain 131 gallons of product. Additionally, 33 gallons of free product has been recovered for a total recovered volume of 164 gallons. Impacted soils are being transported to an approved facility for disposal. Update 7/26/18: final release volume has been calculated based on soil weight tickets and analytical results. 86 tons of soil was excavated and calculated to contain 122 gallons of product. Additionally, 33 gallons of free product was recovered for a total spill volume of 155 gallons.
Detailed record list
Report Received Date
2018-06-25 00:00:00
Iyear
2018
Report Number
20180177
Supplemental Number
31762
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2018-06-11 08:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
3.69
Recovered Bbls
3.69
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-06-11 08:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shut Down Would Not Have Stopped The Leak.
On Site Datetime
2018-06-11 08:00:00
Nrc Rpt Datetime
2018-06-12 09:34:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Danielsville Station
Segment Name
Line 02
Onshore State Abbreviation
Ga
Onshore Postal Code
30628
Onshore City Name
Colbert
Onshore County Name
Madison
Designated Location
Milepost/valve Station
Designated Name
3761
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
M&j
Installation Year
1967
Manufactured Year
1965
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
350
Est Cost Prop Damage
140915
Est Cost Emergency
20000
Est Cost Environmental
12000
Est Cost Other
0
Prpty
173265
Accident Psig
59
Mop Psig
450
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Mechanical seal failure not caused by controller actions.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Station Suction Valve Stem Seal Failure.
Additional Breakdown Ind
Yes
Preparer Name
D***** L******
Preparer Title
Sed Compliance Coordinator
Preparer Email
D*******@c******.com
Preparer Telephone
443-821-1456
Prepared Date
2019-03-08 00:00:00
Authorizer Name
D***** L******
Authorizer Telephone
443-821-1456
Authorizer Title
Sed Compliance Coordinator
Authorizer Email
D*******@c******.com
Narrative
On 6/11/18 at 0800 est, a contract inspector notified the belton lead technician of a stem seal leak on the danielsville station suction valve. After initial notifications, the contract inspector was able to contain the leaking product. The lead technician immediately notified the control center and the lead operator. The lead technician dispatched technician to facility to make repairs and start recovery of spilled product. The lead operator contacted the manager of operations at 0827 est. Director of operations was notified at 0838 and district environmental was notified at 0843 by manager of operations. By 0920, the technician was able to install tubing from the suction valve yoke tube directly to the station sump isolating the leak source as a temporary repair. Contract crews and the district environmental specialist arrived on site at 1130 to assist in recovery. Remedial actions included excavation of contaminated soil and vacuum recovery of any free standing product. On 6/12/18 at 0924 est nrc notification was made when it was determined that the $50,000 notification threshold would be exceeded. Concurrently, a courtesy notification was also made to ga dnr epd - natural recourses operations center and the ga epd case manager for the existing remediation site at the facility. The current estimated release volume is 375 gallons based on estimated time of release and observed rate of release. Final volume of release and recovery will be communicated once excavation is complete and analytical analyses are available. Currently, 80 tons of soil have been excavated and calculated to contain 131 gallons of product. Additionally, 33 gallons of free product has been recovered for a total recovered volume of 164 gallons. Impacted soils are being transported to an approved facility for disposal. Update 7/26/18: final release volume has been calculated based on soil weight tickets and analytical results. 86 tons of soil was excavated and calculated to contain 122 gallons of product. Additionally, 33 gallons of free product was recovered for a total spill volume of 155 gallons.
Report Received Date 2018-06-25 00:00:00
Iyear 2018
Report Number 20180177
Supplemental Number 31762
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2018-06-11 08:00:00
Location Latitude 34.093889 Google Maps OpenStreetMap
Location Longitude -83.233611 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 3.69
Recovered Bbls 3.69
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-06-11 08:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shut Down Would Not Have Stopped The Leak.
On Site Datetime 2018-06-11 08:00:00
Nrc Rpt Datetime 2018-06-12 09:34:00
Nrc Rpt Num 1215019 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Danielsville Station
Segment Name Line 02
Onshore State Abbreviation Ga
Onshore Postal Code 30628
Onshore City Name Colbert
Onshore County Name Madison
Designated Location Milepost/valve Station
Designated Name 3761
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer M&j
Installation Year 1967
Manufactured Year 1965
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 350
Est Cost Prop Damage 140915
Est Cost Emergency 20000
Est Cost Environmental 12000
Est Cost Other 0
Prpty 173265
Accident Psig 59
Mop Psig 450
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Mechanical seal failure not caused by controller actions.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Station Suction Valve Stem Seal Failure.
Additional Breakdown Ind Yes
Preparer Name D***** L******
Preparer Title Sed Compliance Coordinator
Preparer Email D*******@c******.com
Preparer Telephone 443-821-1456
Prepared Date 2019-03-08 00:00:00
Authorizer Name D***** L******
Authorizer Telephone 443-821-1456
Authorizer Title Sed Compliance Coordinator
Authorizer Email D*******@c******.com
Narrative On 6/11/18 at 0800 est, a contract inspector notified the belton lead technician of a stem seal leak on the danielsville station suction valve. After initial notifications, the contract inspector was able to contain the leaking product. The lead technician immediately notified the control center and the lead operator. The lead technician dispatched technician to facility to make repairs and start recovery of spilled product. The lead operator contacted the manager of operations at 0827 est. Director of operations was notified at 0838 and district environmental was notified at 0843 by manager of operations. By 0920, the technician was able to install tubing from the suction valve yoke tube directly to the station sump isolating the leak source as a temporary repair. Contract crews and the district environmental specialist arrived on site at 1130 to assist in recovery. Remedial actions included excavation of contaminated soil and vacuum recovery of any free standing product. On 6/12/18 at 0924 est nrc notification was made when it was determined that the $50,000 notification threshold would be exceeded. Concurrently, a courtesy notification was also made to ga dnr epd - natural recourses operations center and the ga epd case manager for the existing remediation site at the facility. The current estimated release volume is 375 gallons based on estimated time of release and observed rate of release. Final volume of release and recovery will be communicated once excavation is complete and analytical analyses are available. Currently, 80 tons of soil have been excavated and calculated to contain 131 gallons of product. Additionally, 33 gallons of free product has been recovered for a total recovered volume of 164 gallons. Impacted soils are being transported to an approved facility for disposal. Update 7/26/18: final release volume has been calculated based on soil weight tickets and analytical results. 86 tons of soil was excavated and calculated to contain 122 gallons of product. Additionally, 33 gallons of free product was recovered for a total spill volume of 155 gallons.

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