HL incident on 2018-05-17 — TX

Operator
Exxonmobil Pipeline Co
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2018-05-17 07:55
Report number
Location
TX
Narrative
On 5/17/2018 @7:55 a 3rd party operator contacted empco of a possible release at empco's shintech meter site. Empco dispatched technicians and at approximately 08:24 discovered a small ice ball forming on the packing gland housing of an orifice meter. The system was shut-in, and at approximately 12:11 p.M. The system was returned to service following the tightening of a loose packing gland fitting. Empco estimates that approximately 17.11 gallons (0.40 bbls) of ethylene was released. The spill volume was conservatively estimated assuming a continuous release rate, without accounting for any potential flow reduction rate due to observed ice-ball formation, and assumptions regarding the release start time based upon a post-incident identification of local intermittent gas detector indications beginning at approximately 1:01 am and again at approximately 4:27 am.
Detailed record list
Report Received Date
2018-06-15 00:00:00
Iyear
2018
Report Number
20180175
Supplemental Number
31109
Report Type
Supplemental Final
Operator Id
Name
Exxonmobil Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2018-05-17 01:01:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
0.4
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Adjacent Pipeline Operator Personnel Identified The Release And Contacted Empco
Incident Identified Datetime
2018-05-17 07:55:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-05-17 08:24:00
Restart Datetime
2018-05-17 12:11:00
On Site Datetime
2018-05-17 08:24:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Br Ref To Choctaw Ethylene
Segment Name
8" Lateral To Shintech Plant
Onshore State Abbreviation
La
Onshore Postal Code
70765
Onshore City Name
Plaquemine
Onshore County Name
Iberville
Designated Location
Milepost/valve Station
Designated Name
Orifice Meter
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Installation Year
2000
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
9
Est Cost Prop Damage
200
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
209
Accident Psig
1020
Mop Psig
1810
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No investigation was necessary because this was not a controller related release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Leak Tested Packing Became Loose And Failed (Reason Undeterminable).
Preparer Name
K***** L Y****
Preparer Title
Regulatory Compliance Advisor
Preparer Email
K*************@e*********.com
Preparer Telephone
225-324-3055
Prepared Date
2018-10-25 00:00:00
Authorizer Name
C******* B H********
Authorizer Telephone
832-624-7920
Authorizer Title
Americas Fuels Operations Pipeline Sshe Manager
Authorizer Email
C*******************@e*********.com
Narrative
O************@7:55 a 3rd party operator contacted empco of a possible release at empco's shintech meter site. Empco dispatched technicians and at approximately 08:24 discovered a small ice ball forming on the packing gland housing of an orifice meter. The system was shut-in, and at approximately 12:11 p.M. The system was returned to service following the tightening of a loose packing gland fitting. Empco estimates that approximately 17.11 gallons (0.40 bbls) of ethylene was released. ************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************.
Report Received Date 2018-06-15 00:00:00
Iyear 2018
Report Number 20180175
Supplemental Number 31109
Report Type Supplemental Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2018-05-17 01:01:00
Location Latitude 30.24911 Google Maps OpenStreetMap
Location Longitude -91.17552 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 0.4
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Adjacent Pipeline Operator Personnel Identified The Release And Contacted Empco
Incident Identified Datetime 2018-05-17 07:55:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-05-17 08:24:00
Restart Datetime 2018-05-17 12:11:00
On Site Datetime 2018-05-17 08:24:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Br Ref To Choctaw Ethylene
Segment Name 8" Lateral To Shintech Plant
Onshore State Abbreviation La
Onshore Postal Code 70765
Onshore City Name Plaquemine
Onshore County Name Iberville
Designated Location Milepost/valve Station
Designated Name Orifice Meter
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Meter/prover
Installation Year 2000
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 9
Est Cost Prop Damage 200
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 209
Accident Psig 1020
Mop Psig 1810
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No investigation was necessary because this was not a controller related release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Leak Tested Packing Became Loose And Failed (Reason Undeterminable).
Preparer Name K***** L Y****
Preparer Title Regulatory Compliance Advisor
Preparer Email K*************@e*********.com
Preparer Telephone 225-324-3055
Prepared Date 2018-10-25 00:00:00
Authorizer Name C******* B H********
Authorizer Telephone 832-624-7920
Authorizer Title Americas Fuels Operations Pipeline Sshe Manager
Authorizer Email C*******************@e*********.com
Narrative O************@7:55 a 3rd party operator contacted empco of a possible release at empco's shintech meter site. Empco dispatched technicians and at approximately 08:24 discovered a small ice ball forming on the packing gland housing of an orifice meter. The system was shut-in, and at approximately 12:11 p.M. The system was returned to service following the tightening of a loose packing gland fitting. Empco estimates that approximately 17.11 gallons (0.40 bbls) of ethylene was released. ************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************.

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