HL incident on 2018-05-19 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-05-19 08:00
Report number
Location
TX
Narrative
Local operations were notified of oil leaking from the packing on the head gate valve on tank #1441 at 7:15 am; there was no movement scheduled for the tank. Once on site (at 8:00 am) the leak was confirmed and found there was approx. 2 barrels of crude oil released onto the piping and ground. Cleanup and remediation began immediately. Update (9/26/2018): it was discovered that the packing was air locked (stacked) and not sealing off. When the valve was operated, packing was reconfigured and source of leak was eliminated. Also, tank is PHMSA jurisdiction/interstate.
Detailed record list
Report Received Date
2018-06-14 00:00:00
Iyear
2018
Report Number
20180174
Supplemental Number
30980
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-05-19 07:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Notified By Other Operator
Incident Identified Datetime
2018-05-19 08:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Not Being Used To Make Delivery
On Site Datetime
2018-05-19 08:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wichita Falls
Segment Name
Tank 1441
Onshore State Abbreviation
Tx
Onshore Postal Code
76301
Onshore City Name
Wichita Falls
Onshore County Name
Wichita
Designated Location
Milepost/valve Station
Designated Name
Wichita Falls
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Tank Type
Atmospheric
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
130
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
1200
Est Cost Other
0
Prpty
1330
Accident Psig
25
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Ief Addl Misalignment Ind
Yes
Preparer Name
L**** W*******
Preparer Title
Pipeline Compliance Senior Engineer
Preparer Email
L*********@e****.com
Preparer Telephone
713-381-6748
Prepared Date
2018-09-26 00:00:00
Authorizer Name
L**** W*******
Authorizer Telephone
713-381-6748
Authorizer Title
Pipeline Compliance Senior Engineer
Authorizer Email
L*********@e****.com
Narrative
Local operations were notified of oil leaking from the packing on the head gate valve on tank #1441 at 7:15 am; there was no movement scheduled for the tank. Once on site (at 8:00 am) the leak was confirmed and found there was approx. 2 barrels of crude oil released onto the piping and ground. Cleanup and remediation began immediately. Update (9/26/2018): it was discovered that the packing was air locked (stacked) and not sealing off. When the valve was operated, packing was reconfigured and source of leak was eliminated. Also, tank is PHMSA jurisdiction/interstate.
Report Received Date 2018-06-14 00:00:00
Iyear 2018
Report Number 20180174
Supplemental Number 30980
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-05-19 07:15:00
Location Latitude 33.9192 Google Maps OpenStreetMap
Location Longitude -98.4353 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Notified By Other Operator
Incident Identified Datetime 2018-05-19 08:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Not Being Used To Make Delivery
On Site Datetime 2018-05-19 08:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wichita Falls
Segment Name Tank 1441
Onshore State Abbreviation Tx
Onshore Postal Code 76301
Onshore City Name Wichita Falls
Onshore County Name Wichita
Designated Location Milepost/valve Station
Designated Name Wichita Falls
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Tank Type Atmospheric
Installation Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 130
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 1200
Est Cost Other 0
Prpty 1330
Accident Psig 25
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Ief Addl Misalignment Ind Yes
Preparer Name L**** W*******
Preparer Title Pipeline Compliance Senior Engineer
Preparer Email L*********@e****.com
Preparer Telephone 713-381-6748
Prepared Date 2018-09-26 00:00:00
Authorizer Name L**** W*******
Authorizer Telephone 713-381-6748
Authorizer Title Pipeline Compliance Senior Engineer
Authorizer Email L*********@e****.com
Narrative Local operations were notified of oil leaking from the packing on the head gate valve on tank #1441 at 7:15 am; there was no movement scheduled for the tank. Once on site (at 8:00 am) the leak was confirmed and found there was approx. 2 barrels of crude oil released onto the piping and ground. Cleanup and remediation began immediately. Update (9/26/2018): it was discovered that the packing was air locked (stacked) and not sealing off. When the valve was operated, packing was reconfigured and source of leak was eliminated. Also, tank is PHMSA jurisdiction/interstate.

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