HL incident on 2018-05-10 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Other Outside Force Damage
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10
Incident datetime
2018-05-10 07:30
Report number
Location
OK
Narrative
At approximately 7:30 on 5/10/2018 oneok field representative was contacted by contract crew working at oenok's new fall creek junction site to report vapors coming from a 1/2" pipe nipple on a double block and bleed valve on the meter skid. Oneok representative arrived on site at approximately 8:00 am and isolated the valve and removed and replaced the failed pipe nipple. An elevated access platform had been installed prior to heavy rain in the area and as a result of the rainfall, settled in the dirt, allowing the side of the platform to contact the pipe nipple on the double block and bleed valve which caused the nipple to crack causing the release of hydrocarbons. The platform was modified and relocated to prevent a repeat of this type of accident.
Detailed record list
Report Received Date
2018-06-04 00:00:00
Iyear
2018
Report Number
20180164
Supplemental Number
30440
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-05-10 07:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1.45
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-05-10 07:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Isolated And Not In Service At The Time Of The Accident
On Site Datetime
2018-05-10 08:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Fall Creek Jct.
Segment Name
Oneok Site Number 689
Onshore State Abbreviation
Ok
Onshore Postal Code
73044
Onshore City Name
Not Within A Municipality
Onshore County Name
Logan
Designated Location
Milepost/valve Station
Designated Name
Meter Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
10
Est Cost Emergency
112
Est Cost Environmental
0
Est Cost Other
0
Prpty
162
Accident Psig
238
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place prior to the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
Elevated Platform Installed For Access To Valve, Settled Due To Heavy Rain After Installation. When Platform Settled, It Contacted The 1/2" Pipe Nipple On The Double Block And Bleed Valve Causing The Nipple To Fail.
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Manager
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2018-06-04 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
N*********@o****.com
Narrative
At approximately 7:30 on 5/10/2018 oneok field representative was contacted by contract crew working at oenok's new fall creek junction site to report vapors coming from a 1/2" pipe nipple on a double block and bleed valve on the meter skid. Oneok representative arrived on site at approximately 8:00 am and isolated the valve and removed and replaced the failed pipe nipple. An elevated access platform had been installed prior to heavy rain in the area and as a result of the rainfall, settled in the dirt, allowing the side of the platform to contact the pipe nipple on the double block and bleed valve which caused the nipple to crack causing the release of hydrocarbons. The platform was modified and relocated to prevent a repeat of this type of accident.
Report Received Date 2018-06-04 00:00:00
Iyear 2018
Report Number 20180164
Supplemental Number 30440
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2018-05-10 07:30:00
Location Latitude 35.781502 Google Maps OpenStreetMap
Location Longitude -97.23781 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 1.45
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-05-10 07:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Isolated And Not In Service At The Time Of The Accident
On Site Datetime 2018-05-10 08:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Fall Creek Jct.
Segment Name Oneok Site Number 689
Onshore State Abbreviation Ok
Onshore Postal Code 73044
Onshore City Name Not Within A Municipality
Onshore County Name Logan
Designated Location Milepost/valve Station
Designated Name Meter Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 10
Est Cost Emergency 112
Est Cost Environmental 0
Est Cost Other 0
Prpty 162
Accident Psig 238
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place prior to the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Other Outside Force Damage
Outside Force Type Other Outside Force Damage
Osf Other Details Elevated Platform Installed For Access To Valve, Settled Due To Heavy Rain After Installation. When Platform Settled, It Contacted The 1/2" Pipe Nipple On The Double Block And Bleed Valve Causing The Nipple To Fail.
Preparer Name N*** J****
Preparer Title Requlatory Compliance Manager
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2018-06-04 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Manager
Authorizer Email N*********@o****.com
Narrative At approximately 7:30 on 5/10/2018 oneok field representative was contacted by contract crew working at oenok's new fall creek junction site to report vapors coming from a 1/2" pipe nipple on a double block and bleed valve on the meter skid. Oneok representative arrived on site at approximately 8:00 am and isolated the valve and removed and replaced the failed pipe nipple. An elevated access platform had been installed prior to heavy rain in the area and as a result of the rainfall, settled in the dirt, allowing the side of the platform to contact the pipe nipple on the double block and bleed valve which caused the nipple to crack causing the release of hydrocarbons. The platform was modified and relocated to prevent a repeat of this type of accident.

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