HL incident on 2018-04-21 — LA

Operator
Crimson Gulf, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$61,075
Incident datetime
2018-04-21 09:46
Report number
Location
LA
Narrative
Crimson gulf was advised of an unknown source oil sheen near texas petroleum investing company's (tpic) production platform delta duck 3" which ties into crimson's delta north 10" pipeline (la-dn-2). The subsea tie in resides approximately with 8' of water depth and several feet of cover. Tpic placed booms to contain the spotted sheen. Tpic notified crimson at 0946 cst, national response center (nrc), and louisiana department of wildlife and fisheries. Approximately 1200 cst crimson engineering and operations put inshore diving contractors (couvillion group) and environmental cleanup companies (oil mop) on standby. At 1211 cst crimson engineering mobilized couvillion group to begin diving investigation. At 1212 cst the delta north system was disabled from the crimson control center as per request by crimson gulf operations. Crimson sent an emergency permit application to u.S. Fish and wildlife (site is located within delta national wildlife refuge). Notification were made to federal, state, and local agencies. Continuing on the 23rd, divers cleaned the sub-sea assembly bottom and flushed the inside of manifold of the sub-sea assembly. The divers closed the valves to isolate the assembly, pneumatically pressure tested the assembly, and checked for leaks. The air bubbles were noticed coming out of one of the subsea assembly flanges (4). New bolts, nuts and a gasket were installed and properly torqued to repair the leak. Furthermore, the assembly was again pneumatic tested to ensure leak was repaired. After the successful test, water displaced the air out of the assembly, valves were opened, and production came online. Personnel oversight remained on location to visually check the area for a sheen during commissioning and throughout production.
Detailed record list
Report Received Date
2018-06-01 00:00:00
Iyear
2018
Report Number
20180162
Supplemental Number
32114
Report Type
Supplemental Final
Operator Id
Name
Crimson Gulf, Llc
Operator Street Address
263 Trinity Lane
Operator City Name
Gray
Operator State Abbreviation
LA
Operator Postal Code
70359
Local Datetime
2018-04-21 10:30:00
Location Latitude
Location Longitude
-89.19916666
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
3rd Party Operator
Incident Identified Datetime
2018-04-21 09:46:00
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
On Off Shore
Offshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-04-21 12:12:00
Restart Datetime
2018-04-24 14:09:00
On Site Datetime
2018-04-22 08:00:00
Nrc Rpt Datetime
2018-04-21 15:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Off Water Depth
8
Off Accident Origin
In State Waters
Offshore State Abbreviation
La
Off Instate Area
Delta Wildlife Refug
Off Instate Block
70
Offshore County Name
Plaquemines Parish
Off Area Accident Type
Shoreline/bank/marsh Crossing Or Shore Approach
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Ansi 600rtj, Oval Ring Gasket, Soft Iron
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
0.1
Rel Water Name
Gulf Of Mexico Inlet / Marsh Waters
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
61075
Est Cost Emergency
11504
Est Cost Environmental
0
Est Cost Other
0
Prpty
72579
Accident Psig
43
Mop Psig
1224
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
20
Internal Inspection Ind
No
Diameter Change Ind
Yes
Other Restrictions Ind
Yes
Other Inspection Ind
Yes
Internal Inspection Details
10" To 4" Pipe Reduction.
Operation Complications Ind
No
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was from a damaged "o" ring gasket
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Installation Ind
Yes
Preparer Name
D**** B********
Preparer Title
Regulatory Compliance Manager
Preparer Email
D*********@c********.com
Preparer Telephone
562-668-0066
Preparer Fax
562-285-4141
Prepared Date
2019-05-10 00:00:00
Authorizer Name
L*** W A********
Authorizer Telephone
562-285-4100
Authorizer Title
President
Authorizer Email
Lwalexandercrimsonpl.com
Narrative
Crimson gulf was advised of an unknown source oil sheen near texas petroleum investing company's (tpic) production platform delta duck 3" which ties into crimson's delta north 10" pipeline (la-dn-2). The subsea tie in resides approximately with 8' of water depth and several feet of cover. Tpic placed booms to contain the spotted sheen. Tpic notified crimson at 0946 cst, national response center (nrc), and louisiana department of wildlife and fisheries. Approximately 1200 cst crimson engineering and operations put inshore diving contractors (couvillion group) and environmental cleanup companies (oil mop) on standby. At 1211 cst crimson engineering mobilized couvillion group to begin diving investigation. At 1212 cst the delta north system was disabled from the crimson control center as per request by crimson gulf operations. Crimson sent an emergency permit application to u.S. Fish and wildlife (site is located within delta national wildlife refuge). Notification were made to federal, state, and local agencies. Continuing on the 23rd, divers cleaned the sub-sea assembly bottom and flushed the inside of manifold of the sub-sea assembly. The divers closed the valves to isolate the assembly, pneumatically pressure tested the assembly, and checked for leaks. The air bubbles were noticed coming out of one of the subsea assembly flanges (4). New bolts, nuts and a gasket were installed and properly torqued to repair the leak. Furthermore, the assembly was again pneumatic tested to ensure leak was repaired. After the successful test, water displaced the air out of the assembly, valves were opened, and production came online. Personnel oversight remained on location to visually check the area for a sheen during commissioning and throughout production.
Report Received Date 2018-06-01 00:00:00
Iyear 2018
Report Number 20180162
Supplemental Number 32114
Report Type Supplemental Final
Operator Id 39084 PHMSA Enforcement
Name Crimson Gulf, Llc
Operator Street Address 263 Trinity Lane
Operator City Name Gray
Operator State Abbreviation LA
Operator Postal Code 70359
Local Datetime 2018-04-21 10:30:00
Location Latitude 29.26083333 Google Maps OpenStreetMap
Location Longitude -89.19916666 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details 3rd Party Operator
Incident Identified Datetime 2018-04-21 09:46:00
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
On Off Shore Offshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-04-21 12:12:00
Restart Datetime 2018-04-24 14:09:00
On Site Datetime 2018-04-22 08:00:00
Nrc Rpt Datetime 2018-04-21 15:26:00
Nrc Rpt Num 1210217 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Off Water Depth 8
Off Accident Origin In State Waters
Offshore State Abbreviation La
Off Instate Area Delta Wildlife Refug
Off Instate Block 70
Offshore County Name Plaquemines Parish
Off Area Accident Type Shoreline/bank/marsh Crossing Or Shore Approach
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Ansi 600rtj, Oval Ring Gasket, Soft Iron
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Ocean Seawater Ind Yes
Amount Released 0.1
Rel Water Name Gulf Of Mexico Inlet / Marsh Waters
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 61075
Est Cost Emergency 11504
Est Cost Environmental 0
Est Cost Other 0
Prpty 72579
Accident Psig 43
Mop Psig 1224
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 20
Internal Inspection Ind No
Diameter Change Ind Yes
Other Restrictions Ind Yes
Other Inspection Ind Yes
Internal Inspection Details 10" To 4" Pipe Reduction.
Operation Complications Ind No
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was from a damaged "o" ring gasket
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Additional Installation Ind Yes
Preparer Name D**** B********
Preparer Title Regulatory Compliance Manager
Preparer Email D*********@c********.com
Preparer Telephone 562-668-0066
Preparer Fax 562-285-4141
Prepared Date 2019-05-10 00:00:00
Authorizer Name L*** W A********
Authorizer Telephone 562-285-4100
Authorizer Title President
Authorizer Email Lwalexandercrimsonpl.com
Narrative Crimson gulf was advised of an unknown source oil sheen near texas petroleum investing company's (tpic) production platform delta duck 3" which ties into crimson's delta north 10" pipeline (la-dn-2). The subsea tie in resides approximately with 8' of water depth and several feet of cover. Tpic placed booms to contain the spotted sheen. Tpic notified crimson at 0946 cst, national response center (nrc), and louisiana department of wildlife and fisheries. Approximately 1200 cst crimson engineering and operations put inshore diving contractors (couvillion group) and environmental cleanup companies (oil mop) on standby. At 1211 cst crimson engineering mobilized couvillion group to begin diving investigation. At 1212 cst the delta north system was disabled from the crimson control center as per request by crimson gulf operations. Crimson sent an emergency permit application to u.S. Fish and wildlife (site is located within delta national wildlife refuge). Notification were made to federal, state, and local agencies. Continuing on the 23rd, divers cleaned the sub-sea assembly bottom and flushed the inside of manifold of the sub-sea assembly. The divers closed the valves to isolate the assembly, pneumatically pressure tested the assembly, and checked for leaks. The air bubbles were noticed coming out of one of the subsea assembly flanges (4). New bolts, nuts and a gasket were installed and properly torqued to repair the leak. Furthermore, the assembly was again pneumatic tested to ensure leak was repaired. After the successful test, water displaced the air out of the assembly, valves were opened, and production came online. Personnel oversight remained on location to visually check the area for a sheen during commissioning and throughout production.

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